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航空航天铝合金构件装配孔钻削出口毛刺研究进展
引用本文:王笑时,杨国林,董志刚,康仁科.航空航天铝合金构件装配孔钻削出口毛刺研究进展[J].金刚石与磨料磨具工程,2022,42(4):385-409.
作者姓名:王笑时  杨国林  董志刚  康仁科
作者单位:大连理工大学,精密与特种加工教育部重点实验室,辽宁 大连 116024
摘    要:航空航天制造业中存在大量的铝合金装配孔加工需求。装配孔主要通过钻削加工实现,加工中存在铝合金出口毛刺过大的问题。出口毛刺直接影响工件的精度、抗疲劳强度、装配性能,去毛刺工序会极大地增加工时和成本。因此有必要对铝合金装配孔钻削出口毛刺进行研究,实现对出口毛刺的控制。从铝合金钻削出口毛刺的类型和测量方法、形成机理和高度预测以及毛刺控制方法等方面进行了系统性的论述,以期为铝合金钻削加工出口毛刺的研究提供帮助。 

关 键 词:铝合金    钻削    出口毛刺    形成机理    控制方法
收稿时间:2021-12-27

Research progress on exit burr in drilling assembly hole of aerospace aluminum alloy components
WANG Xiaoshi,YANG Guolin,DONG Zhigang,KANG Renke.Research progress on exit burr in drilling assembly hole of aerospace aluminum alloy components[J].Diamond & Abrasives Engineering,2022,42(4):385-409.
Authors:WANG Xiaoshi  YANG Guolin  DONG Zhigang  KANG Renke
Affiliation:Key Laboratory for Precision and Non-traditional Machining Technology of Ministry of Education, Dalian University of Technology, Dalian 116024, Liaoning, China
Abstract:There is a large demand for aluminum alloy assembly hole machining in aerospace manufacturing industry. The assembly hole is mainly realized by drilling, and there is a problem that the aluminum alloy exit burr is too large in the processing. The exit burr directly affects the accuracy, fatigue strength and assembly performance of the workpiece. The deburring process will greatly increase the man hour and cost. Therefore, it is necessary to study the exit burr of aluminum alloy assembly hole drilling to realize the control of exit burr. This paper systematically discusses the types, measurement methods, formation mechanism, height prediction and gross control methods of exit burr in aluminum alloy drilling, in order to provide help for the research of exit burr in aluminum alloy drilling. 
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