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1.
Can Ercan S. Esra Safran Artuğ Türkmenoğlu Uğur Karabakal 《Journal of surfactants and detergents》2021,24(1):139-147
Garzan oil field is located at the south east of Turkey. It is a mature oil field and the reservoir is fractured carbonate reservoir. After producing about 1% original oil in place (OOIP) reservoir pressure started to decline. Waterflooding was started in order to support reservoir pressure and also to enhance oil production in 1960. Waterflooding improved the oil recovery but after years of flooding water breakthrough at the production wells was observed. This increased the water/oil ratio at the production wells. In order to enhance oil recovery again different techniques were investigated. Chemical enhanced oil recovery (EOR) methods are gaining attention all over the world for oil recovery. Surfactant injection is an effective way for interfacial tension (IFT) reduction and wettability reversal. In this study, 31 different types of chemicals were studied to specify the effects on oil production. This paper presents solubility of surfactants in brine, IFT and contact angle measurements, imbibition tests, and lastly core flooding experiments. Most of the chemicals were incompatible with Garzan formation water, which has high divalent ion concentration. In this case, the usage of 2-propanol as co-surfactant yielded successful results for stability of the selected chemical solutions. The results of the wettability test indicated that both tested cationic and anionic surfactants altered the wettability of the carbonate rock from oil-wet to intermediate-wet. The maximum oil recovery by imbibition test was reached when core was exposed 1-ethly ionic liquid after imbibition in formation water. Also, after core flooding test, it is concluded that considerable amount of oil can be recovered from Garzan reservoir by waterflooding alone if adverse effects of natural fractures could be eliminated. 相似文献
2.
《International Journal of Hydrogen Energy》2022,47(9):6377-6387
This work is focused on the explosion characteristics of premixed gas containing different volume fractions of hydrogen in a narrow channel (1000 mm × 50 mm × 10 mm) under the circumstance of stoichiometric ratio. The ignition positions were set in the closed end and the middle of the pipeline respectively. The results showed that when the gas was ignited at the pipeline closed end, the propagating flame was tulip structure for different premixed gas. When the hydrogen volume fraction was less than 40%, the flame propagation speed increased significantly with the rise of hydrogen volume fraction, and the overpressure peak also appeared obviously in advance. However, when the volume fraction of hydrogen was more than 40%, the increase of flame propagation speed and the overpressure peak occurrence time varied slightly. Furthermore, when the ignition position was placed in the middle of the pipeline, the flame propagation speed propagating to the opening end was much faster than that propagating to the closing end, and there was no tulip shape when the flame propagates to the opening end. The flame propagating to the closed end appeared tulip shape under the influence of airflow, and high-frequency flame oscillation occurred during the propagation. This work shows that the hydrogen volume fraction and ignition position significantly affected the flame structure, flame front speed, and explosion overpressure. 相似文献
3.
Electric nanogenerators that directly convert the energy of moving drops into electrical signals require hydrophobic substrates with a high density of static electric charge that is stable in “harsh environments” created by continued exposure to potentially saline water. The recently proposed charge-trapping electric generators (CTEGs) that rely on stacked inorganic oxide–fluoropolymer (FP) composite electrets charged by homogeneous electrowetting-assisted charge injection (h-EWCI) seem to solve both problems, yet the reasons for this success have remained elusive. Here, systematic measurements at variable oxide and FP thickness, charging voltage, and charging time and thermal annealing up to 230 °C are reported, leading to a consistent model of the charging process. It is found to be controlled by an energy barrier at the water-FP interface, followed by trapping at the FP-oxide interface. Protection by the FP layer prevents charge densities up to −1.7 mC m−2 from degrading and the dielectric strength of SiO2 enables charge decay times up to 48 h at 230 °C, suggesting lifetimes against thermally activated discharging of thousands of years at room temperature. Combining high dielectric strength oxides and weaker FP top coatings with electrically controlled charging provides a new paradigm for developing ultrastable electrets for applications in energy harvesting and beyond. 相似文献
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5.
《International Journal of Hydrogen Energy》2022,47(8):5638-5649
The sustainable reduction of greenhouse gas emissions from road transport requires solutions to achieve net-zero carbon dioxide emissions. Therefore, in addition to vehicles with electrified powertrains, such as those implemented in battery electric of fuel cell vehicles, internal combustion engines fueled with e-fuels or biofuels are also under discussion. An e-fuel that has come into focus recently, is hydrogen due to its potential to achieve zero tank-to-wheel and well-to-wheel carbon dioxide emissions when the electrolysis is powered by electricity from renewable sources. Due to the high laminar burning velocity, hydrogen has the potential for engine operation with high cylinder charge dilution by e.g. external exhaust gas recirculation or enleanment, resulting in increased efficiency. On the other hand, the high burning velocity and high adiabatic flame temperatures pose a challenge for engine cooling due to increased heat losses compared to conventional fuels. To further evaluate the use of hydrogen for small passenger car engines, a series production 1 L 3 cylinder gasoline engine provided by Ford Werke GmbH was modified for hydrogen direct injection. The engine was equipped with a high pressure external exhaust gas recirculation system to investigate charge dilution at stoichiometric operation. Due to limitations of the turbocharging system, very lean operation, which can achieve nitrogen oxides raw emissions below 10 ppm, was limited to part load operation below BMEP = 8 bar. Thus, a reduction of the nitrogen oxides emission level at high loads compared to stoichiometric operation was not possible. At stoichiometric operation with external exhaust gas recirculation engine efficiency can be increased significantly. The comparison of stoichiometric hydrogen and gasoline operation shows a reduced indicated efficiency with hydrogen with significant faster combustion of hydrogen at comparable centers of combustion. However, higher boost pressures would allow to achieve even higher indicated efficiencies by charge dilution compared to gasoline engine operation. 相似文献
6.
目的:探索炎性疾病患者的乳酸林格氏液(Ringer's lactate,RL)液体动力学特征以及炎性生物标记物是否可以作为协变量影响RL分布和排泄。方法:本研究为前瞻性队列研究。选择40例美国麻醉医师分级(ASA)I-II级,腹腔镜下择期胆囊切除术(胆囊炎组,n=20)或者腹腔镜下急诊阑尾切除术(阑尾炎组,n=20)。所有患者麻醉诱导前开始输注RL,按15 mL/kg,35 min内输毕。采用酶联免疫(enzyme-linked immunosorbent assay,ELISA)方法测定血浆炎症(TNF-α,IL-10和CRP)或者内皮损伤生物标记物(syndecan-1,SDC-1);利用血红蛋白(Hb)稀释-时间曲线和尿量,使用Phoenix软件,采用非线性混合效应模型分析计算RL液体动力学参数和协变量的影响。结果:与胆囊炎组相比,阑尾炎组RL从组织间隙到血浆的转运速率常数(k21)显著降低(14×10-3min-1 versus 35×10-3min-1;P=0.012)。阑尾炎组C反应蛋白(CRP)升高[中位数38.1(1.8-143.6) μg/mL versus 1.3(0.1-159.0) μg/mL;P<0.001];与清醒状态相比,麻醉期间(输液开始后30~45 min),液体从中央室中到外周室的转运速率常数(k12)显著增加(57×10-3min-1 versus 32×10-3min-1;P<0.01)。清除速率常数(k10)降低90%(0.6×10-3min-1 versus 5.3×10-3min-1;P<0.001)。无论在清醒状态还是麻醉状态下低血压均能降低液体清除;炎症或者内膜损伤的生物标记物不能作为显著影响RL液体动力学参数的协变量。结论:阑尾炎或者胆囊炎患者术前输入液体后“炎症反应的生物标记物”不是RL的液体动力学的协变量,但是两组患者中,全身麻醉期间输入液体的清除率下降。 相似文献
7.
结合B超扫描仪支架塑件的形状特点,通过合理地选择塑件的分型面,简化了塑件的整体结构设计及脱模机构设计。针对塑件上脱模需要的复杂性,设计了一种五滑块联动机构先实施内壁5个倒扣及内壁凹形部位内壁的脱模;而后通过2个斜导柱滑块机构来实施外壁的脱模及侧端的侧孔抽芯脱模,塑件最后由推管顶出来实施最终的完全脱模。配合于脱模机构的动作需要,模架选用三板式模架,模架第一次打开设置用于驱动五滑块联动机构的抽芯动作,第二次打开设置用于驱动外壁及侧端的斜导柱驱动侧滑块机构的抽芯动作。五滑块联动机构设计中,通过一个中央T形槽驱动块,驱动中间过渡滑块,从而通过燕尾槽联结来带动5个成型滑块做内收式抽芯运动,巧妙地解决了塑件上局部区域内设置多个抽芯机构设计空间不够的问题,保证了塑件的自动化注塑生产的可靠实现。 相似文献
8.
《低温学》2015
The development of a high cooling power and high efficiency 4.2 K two stage G-M cryocooler is critically important given its broad applications in low temperature superconductors, MRI, infrared detector and cryogenic electronics. A high efficiency 1.5 W/4.2 K pneumatic-drive G-M cryocooler has recently been designed and developed by ARS. The effect of expansion volume rate and operation conditions on the cooling performance has been experimentally investigated. A typical cooling performance of 1.5 W/4.2 K has been achieved, and the minimum temperature of the second stage is 2.46 K. The steady input power of the compressor at 60 Hz is 6.8 kW, while the operation speed of the rotary valve is 30 rpm. A maximum cooling power of 1.75 W/4.2 K has been obtained in test runs. 相似文献
9.
利用模糊控制和比例积分微分(PID)控制相结合的手段对注塑机料筒温度进行了控制,同时以Matlab 6.0软件为仿真平台,对料筒温度控制进行了模拟仿真研究。实验发现,在注塑机料筒升温过程中利用CHR整定的PID控制手段和模糊控制手段,恒温过程中利用人工整定的PID控制手段,可保证快速的料筒升温响应速率和稳定的保温过程。通过实际注塑实验对该仿真结果进行了验证,在十组实验中,料筒温度误差不超过2%,产品翘曲变形量不超过0.059 mm。 相似文献
10.