首页 | 本学科首页   官方微博 | 高级检索  
     

响洪甸水库坝基扬压力异常原因及处理方法的探讨
引用本文:胡子俊.响洪甸水库坝基扬压力异常原因及处理方法的探讨[J].大坝与安全,2007(4):39-43.
作者姓名:胡子俊
作者单位:响洪甸水电站,安徽,金寨,237335
摘    要:响洪甸水库大坝被评定为三类坝,其最主要原因是该库的防洪能力不足、大坝坝基扬压力过高和F2断层难以确定,严重影响大坝的安全稳定.本文主要对坝基扬压力过高的探查试验情况进行介绍,对产生的原因进行分析,并提出了处理方案的设想.

关 键 词:响洪甸水库  扬压力  偏高  原因分析  处理建议
文章编号:1671-1092(2007)04-0039-05
修稿时间:2007-04-28

Cause analysis of dam foundation uplift pressure anomaly and treatment methods
HU Zi-jun.Cause analysis of dam foundation uplift pressure anomaly and treatment methods[J].Large Dam & Safety,2007(4):39-43.
Authors:HU Zi-jun
Affiliation:HU Zi-jun Xianghongdian Hydropower Plant
Abstract:Because of low flood prevention ability,higher dam foundation uplift pressure than standard and the uncertainty of the fault F2,dam safety and stability was effected.As a result,Xianghongdian reservoir dam was classified as Grade 3.This paper introduced the investigation test of dam foundation uplift pressure,analysed the cause reason and advanced the treatment advice.
Keywords:Xianghongdian reservoir  uplift pressure  higher from standard  cause analysis  treatment advice
本文献已被 CNKI 维普 万方数据 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号