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丘东气田修正等时试井优化设计探讨
引用本文:刘雄飞.丘东气田修正等时试井优化设计探讨[J].油气井测试,2000,9(4):69-72.
作者姓名:刘雄飞
作者单位:吐哈油田井下技术作业公司
摘    要:丘东气田是低渗储层年气田,采用修正等时试井方法较为合理。经在温1井、温8-26井实施修正等时试井工艺,提出了气井修正等时试井的优化方案,包括等时间隔的选取、延时生产时间的确定、气井产量的确定、生产管径的影响、井筒容积的影响、压力计下深及施工过程 的监测几方面,以供同类气井产能试井借鉴。

关 键 词:吐鲁番盆地  凝析气田  修正等时试井  优化设计

Probing into the Optimizing Design of Modified Isochronal Flow Test in Qiu Dong Gas Field
Liu Xiongfei.Probing into the Optimizing Design of Modified Isochronal Flow Test in Qiu Dong Gas Field[J].Well Testing,2000,9(4):69-72.
Authors:Liu Xiongfei
Abstract:Qiudong gas field is the condensate gas field with low permeability reservoir,which is comparatively reasonable to adopt the modified isochronal flow test method.Having been used this technology at Wen 1 well,Wen 8 26 well,the optimizing design of gas well has been proposed that includes selecting time intervals,determining prolong production time,defining the gas production effect of production calibre,effect of well bore volume,depth of lowing gauge and monitor in the operation process.All of this provide a reference for the same kind of gas field production test.
Keywords:Tulufan Basin  condensate field  modified isochronal flow test  optimizing design  
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