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井下自生气复合泡沫技术在稠油热采中的研究与应用
引用本文:姚凯,王史文,孙明磊,党龙梅,刘艳波.井下自生气复合泡沫技术在稠油热采中的研究与应用[J].特种油气藏,2002,9(1):61-63.
作者姓名:姚凯  王史文  孙明磊  党龙梅  刘艳波
作者单位:中石化胜利油田股份有限公司现河采油厂,山东,东营,257015
摘    要:针对乐安稠油老区吞吐末期开发效果日益变差的状况,开展了井下自生气复合泡沫技术研究。根据室内研究,在高温下引发剂迅速分解产生的CO2等气体,能扩大蒸汽扫油面积,降低原油粘度,提高注汽效果。当引发剂与泡沫剂混合注入时,则兼具气驱、活性液驱与泡沫驱的功效。该工艺现场施工简单,费用低,在草20区块开展了3口井的现场应用试验,收到了较好的增油效果。

关 键 词:特稠油  引发剂  发泡剂  气驱  活性液驱  泡沫驱  乐安油田  热力采油  驱油
文章编号:1006-6535(2002)01-0061-03
修稿时间:2001年10月15

Study and application of downhole authigenic gas compound foam in heavy oil thermal recovery
YAO Kai,WANG Shi wen,SUN Ming lei,LIU Yan bo,DANG Long mei.Study and application of downhole authigenic gas compound foam in heavy oil thermal recovery[J].Special Oil & Gas Reservoirs,2002,9(1):61-63.
Authors:YAO Kai  WANG Shi wen  SUN Ming lei  LIU Yan bo  DANG Long mei
Abstract:In accordance with the problem of worse becoming development in late period of steam stimulation in old heavy oil area of Lean oilfield, study on downhole authigenic gas compound foam has been carried out. Laboratory study discovered that CO\-2 and other gases generated from rapid decomposition of initiating agent under high temperature could expand steam sweep area, reduce oil viscosity, and improve steam injection efficiency. When initiating agent and foaming agent were injected together, there showed effectiveness of gas drive, surfactant flood and foam drive. This technology is simple and cheap. Field application in 3 wells of block Cao 20 had resulted in favorable production increment.
Keywords:extra  heavy oil  initiating agent  foaming agent  gas drive  surfactant flood  foam drive  Lean oilfield  
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