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超低渗油藏注气采油可行性实验
引用本文:孙黎娟,吴凡,刘社芹,张素芹,荣桂花,王瑞华.超低渗油藏注气采油可行性实验[J].石油地质与工程,2005,19(3):38-39.
作者姓名:孙黎娟  吴凡  刘社芹  张素芹  荣桂花  王瑞华
作者单位:中国石油大学(华东)山东东营257061;中原油田分公司勘探开发科学研究院;中原油田分公司勘探开发科学研究院
摘    要:超低渗油藏由于孔喉极细,即使高压注水,也难以保持注采平衡,应考虑注气的可行性。文中进行了水驱油和氮气驱油试验,以比较驱替效果,探究超低渗油藏的驱替机理。结果表明,对于小于1×10-3μm2的超低渗岩心,气驱比水驱效果好,气驱平均采收率为27.9%,水驱平均采收率为24.1%。说明注气具有一定的优越性。

关 键 词:超低渗油藏  注采平衡  注气  可行性  水驱油  气驱油  采收率
文章编号:1006-4095(2005)03-0038-02
修稿时间:2005年3月25日

Experimental study of feasibility of gas injection recovery in ultra- low permeability reservoirs
Sun Lijuan et al.Experimental study of feasibility of gas injection recovery in ultra- low permeability reservoirs[J].Petroleum Geology and Engineering,2005,19(3):38-39.
Authors:Sun Lijuan
Abstract:To maintain a balanced injection and production rate in ultra - low permeability reservoirs is very difficult even when applying a very high pressure water injection, due to the very fine pore throats, therefore the feasibility of gas injection should be considered. Water - drive and nitrogen - drive experiments are performed to compare their displacement effects and study the displacing mechanism of ultra - low permeability reservoirs. In core with an ultra - low permeability of 1×10-3μm2 , the average recovery factor of gas drive is 27. 9% , 3. 8 percentage points higher than the 24. 2% of water drive, indicating that gas drive is advantageous to some extent.
Keywords:ultra -low permeability reservoir  balanced injection and production rate  gas injection  feasibility  water drive  gas drive  recovery factor  
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