首页 | 本学科首页   官方微博 | 高级检索  
     

曝气生物滤池对CODCr去除效果的试验研究
引用本文:杨青,赵玉华,周晴,傅金祥,陈正清.曝气生物滤池对CODCr去除效果的试验研究[J].沈阳建筑工程学院学报(自然科学版),2005,21(2):138-141.
作者姓名:杨青  赵玉华  周晴  傅金祥  陈正清
作者单位:沈阳建筑大学市政与环境工程学院,辽宁沈阳110168
基金项目:辽宁省自然基金项目(20022007)
摘    要:目的 研究升流式二级曝气生物滤池工艺对生活污水中CODCr的去除效果,为其推广应用提供参考依据.方法 该工艺使用的一级填料为陶粒,二级填料为片状活性炭.采用改变滤速、各级曝气量等工艺参数,对比了CODCr在不同阶段的处理效果.结果 反应器在1~2m/h滤速下自然挂膜成功,在3~5m/h滤速时CODCr去处效果稳定.结论 在流速3m/h、曝气量25L/h时,CODQ处理效果稳定,总平均去除率近90%.当流速为4m/h、曝气量37.5L/h时,去除率为88.20%.滤速5m/h时,一级的曝气量由37.5L/h提高至50L/h,由于较大的上升水流与气流的共同扰动作用增大了滤层孔隙,致使反应器对CODn的去除率有所下降.并采用气、水联合反冲洗,除去老化的生物膜和截留的悬浮物.

关 键 词:CODCr  曝气生物滤池  去除效果  试验研究  处理效果  曝气量  去除率  生活污水  推广应用  工艺参数  扰动作用  上升水流  反应器  滤速  升流式  活性炭  反冲洗  悬浮物  生物膜  二级  填料  流速  挂膜
文章编号:1671-2021(2005)02-0138-04
修稿时间:2004年8月15日

Biological Aerated Filter for Removal of CODCr
YANG Qing,ZHAO Yu-hua,ZHOU Qing,FU Jin-xiang,CHEN Zheng-qing.Biological Aerated Filter for Removal of CODCr[J].Journal of Shenyang Archit Civil Eng Univ: Nat Sci,2005,21(2):138-141.
Authors:YANG Qing  ZHAO Yu-hua  ZHOU Qing  FU Jin-xiang  CHEN Zheng-qing
Abstract:In the study,two-stage biological aerated filter was carried out to treat domestic wastewater in dynamic experiment.The COD_(Cr) removal effective of this treatment craft was investigated.The first filter was filled with ceramist,and the second was laminated activated carbon.By comparing the rate of COD_(Cr) in different phases by changing several craftwork parameters,the results showed the reactor bio-adhered successfully during the velocity of 1?m/h to 2?m/h and got a stable remove-rate of COD_(Cr) during the velocity of 3?m/h to 5?m/h.Therefore,it is safe to draw the conclusion that when the velocity of flow is 3?m/h and the aerate is at 25?L/h,the rate of the COD_(Cr) removal keeps stably and the total average removal rate is near to 90%.The rate reaches at 88.2%,when the velocity is 4?m/h and the aerate 37.5?L/h.At the 5?m/h velocity when the aerate raises from 37.5?L/h to 50?L/h in the first filter,the rate of the COD_(Cr) removal declines for some extent because of the enlarged holes between the filters caused by the fierce current and airflow churning up.The treatment effective will refresh after 10 to 15 minutes back washing of aerate and water.The back-washing cycle of the first filter is 1to 2 days,while that of the second is 3 to 4days.
Keywords:biological aerated filter (BAF)  ceramist  activated carbon  domestic wastewater  COD_(cr)
本文献已被 CNKI 维普 万方数据 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号