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广州抽水蓄能电站二期工程钢筋混凝土岔管高压渗水的处理及有关问题探讨
引用本文:刘学山.广州抽水蓄能电站二期工程钢筋混凝土岔管高压渗水的处理及有关问题探讨[J].广东电力,2006,19(6):39-42.
作者姓名:刘学山
作者单位:广东蓄能发电有限公司,广州,510630
摘    要:广州抽水蓄能电站二期工程(以下简称为广蓄二期)于1998年建成,在上游水道首次充水时,位于上游水道系统的钢筋混凝土岔管上方的排水探洞出现了的高压渗水,最大渗水量达31.78L/s。水道放空后,采用高压化学灌浆和回填高压钢筋混凝土岔管上方的排水探洞,对高压渗水进行了成功处理,目前电站已安全运行了约7年,高岔区的总渗水量一直稳定在2.3L/s。

关 键 词:广蓄二期  钢筋混凝土岔管  限裂设计  最小主应力  追踪劈裂  临界水力梯度
文章编号:1007-290X(2006)06-0039-04
收稿时间:2006-02-07
修稿时间:2006年2月7日

Study on treatment and relevant problems of HP leakage in reinforced concrete manifold of Guangzhou Pumped Storage Power Station Phase-Ⅱ project
LIU Xue-shan.Study on treatment and relevant problems of HP leakage in reinforced concrete manifold of Guangzhou Pumped Storage Power Station Phase-Ⅱ project[J].Guangdong Electric Power,2006,19(6):39-42.
Authors:LIU Xue-shan
Affiliation:Guangdong Pumped Storage Co. , Ltd. , Guangzhou 510630. China
Abstract:The second-stage project of Guangzhou Pumped Storage Power Station was completed in 1998.During the initial water filling of the upstream tunnel,high-pressure water seepage occurred in the drainage tunnel located above the reinforced concrete manifold in the upstream tunnel system,maximal rate of the leakage reaching 31.78 L/s.The leakage was successfully treated through HP chemical grouting and backfilling the drainage tunnel after emptying.Now the power station has been operating safely for about seven years with the leakage rate near the manifold stabilizing at 2.3 L/s.
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