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直流输电系统接地极线路导线脱落事故原因分析及防范措施
引用本文:祝永坤,刘奎,宋建山.直流输电系统接地极线路导线脱落事故原因分析及防范措施[J].内蒙古电力技术,2014,32(6):111-113.
作者姓名:祝永坤  刘奎  宋建山
作者单位:1. 国网内蒙古东部电力有限公司,呼和浩特,010020
2. 国网内蒙古东部电力有限公司兴安供电公司,内蒙古乌兰浩特,137400
3. 乌兰察布察右后旗农电公司,内蒙古乌兰察布,021008
摘    要:500 k V伊穆直流输电系统接地极线路导线发生绝缘子炸裂、导线落地事故,由于接地极线路招弧角放电间隙过小,导致直流系统在操作过电压作用下产生燃弧现象。直流系统无法熄弧是造成事故的主要原因,对此提出了加大招弧角放电间隙、调整接地极线路绝缘配置等防范措施。

关 键 词:直流输电系统  接地极线路导线  燃弧  招弧角  放电间隙  绝缘配置

Fall-down Fault Analysis on Grounding Line Conductor of Direct Current Transmission Line and Its Preventive Measures
Zhu Yongkun,Liu Kui,Song Jianshan.Fall-down Fault Analysis on Grounding Line Conductor of Direct Current Transmission Line and Its Preventive Measures[J].Inner Mongolia Electric Power,2014,32(6):111-113.
Authors:Zhu Yongkun  Liu Kui  Song Jianshan
Affiliation:Zhu Yongkun, Liu Kui, Song Jianshan(1. Grid East Inner Mongolia Electric Power Company Limited, Hohhot 010020; 2.Xing'an Power Supply Bureau, Inner Mongolia Ulanhot 137400; 3.Qahar Right Wing Rear Banner Power Supply Bureau, Inner Mongolia 021008)
Abstract:According to the 500 kV Gimo HVDC ground electrode insulator, conductor ground crack fault, analysis of grounding line arcing horn discharge gap which was too small in the operating over voltage under the effect of arc, DC system couldn't extinguish the arc, which was the main cause of the ground wire insulator crack, then put forward preventive measures to increase the arcing horn discharge gap, adjusting the ends of the earth line insulation configuration and other means.
Keywords:DC transmission system  grounding line conductor  arcing  trick arc angle  discharge gap  insulation configuration
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