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定向井抽油杆柱应力分析及加重杆的应用
引用本文:徐永高,黎晓茸,王喜兵,甘庆明.定向井抽油杆柱应力分析及加重杆的应用[J].石油矿场机械,2009,38(7):50-52.
作者姓名:徐永高  黎晓茸  王喜兵  甘庆明
作者单位:1. 中国石油长庆油田分公司油气工艺研究院,西安,710018
2. 中国石油长庆油田分公司第一采油厂,陕西延安,716000
摘    要:长庆油田目前的定向井井数达到了总井数的85%以上。由于定向井井眼轨迹的特殊性,抽油杆在油井内的受力情况比较复杂,很容易出现断脱问题,严重影响了油井正常生产。分析了定向井抽油杆柱的弯曲应力及其影响;进行了加重杆的优化设计。抽油杆柱下部配加重杆的方法经现场应用后取得了较好的效果,延长了油井免修期,目前已全面推广应用。

关 键 词:定向井  杆柱组合  加重杆  应力分析

Stress Analysis of Sucker Rod and Application of Heavy-weight Rod in Directional Well
XU Yong-gao,LI Xiao-rong,WANG Xi-bing,GAN Qing-ming.Stress Analysis of Sucker Rod and Application of Heavy-weight Rod in Directional Well[J].Oil Field Equipment,2009,38(7):50-52.
Authors:XU Yong-gao  LI Xiao-rong  WANG Xi-bing  GAN Qing-ming
Affiliation:XU Yong-gao , LI Xiao-rong , WANG Xi-bing , GAN Qing-ming ( 1. Oil & Gas Technology Research Institute, Changqing Oil field of CNPC, Xi ' an 710018, China ; 2. No. 1 Oil Production Plant ,Changqing Oil field of CNPC , Yanan 716000,China)
Abstract:Changqing field is located in rough loess plateau area. Recently, in order to save ground surface construction cost and have easy management, cluster wells were drilled directionally in large area and the ratio of directional wells was up to 85%. In the process of production due to peculiarity of well holes, the stress of pumping rods had changed so complex that they would break and slip easily, thus wells production had been damaged. We have taken many measures to solve this problem and weighing under the rod was one of these solutions. After theoretical calcu-lation and field tests the method has been applied extensively and confirmed that it has good effect and can prolong well repair free period.
Keywords:directional well  sucker rod combination  weighing rod  stress analysis
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