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稠油热采井新型增效技术的现场实践及认识
引用本文:谢建军,魏淋生,赵长喜,王新亮,王晓东.稠油热采井新型增效技术的现场实践及认识[J].石油地质与工程,2007,21(2):65-68.
作者姓名:谢建军  魏淋生  赵长喜  王新亮  王晓东
作者单位:1. 长江大学,湖北荆州,434023;中国石化河南油田分公司石油工程技术研究院
2. 中国石化河南油田分公司石油工程技术研究院
基金项目:中国石油化工集团公司资助项目
摘    要:针对稠油高周期吞吐开发后期蒸汽热效率低的问题,研究出新型蒸汽增效剂及施工工艺,利用分解气体和表面活性剂的协同作用,可使非均质岩心驱油效率平均提高16.5%。采用井口多段塞注入和伴蒸汽滴注工艺,在河南油田、胜利油田和克拉玛依油田现场应用了120多口井,有效率达到92.5%。现场实践证明,新型蒸汽增效剂具有增加地层能量、提高蒸汽波及体积和驱油效率多重功效,能够显著提高热采井的产量,但对于高含水(大于85%)、存在严重汽窜的地层,还具有一定局限性。

关 键 词:稠油热采  新技术  现场应用  认识
文章编号:1673-8217(2007)02-0065-04
修稿时间:2006年12月12

Field trials and views of new technique for raising the production in thermal recovery well
Xie Jianjun.Field trials and views of new technique for raising the production in thermal recovery well[J].Petroleum Geology and Engineering,2007,21(2):65-68.
Authors:Xie Jianjun
Abstract:In view of the low efficiency of high circle stimulation in later period of heavy-oil development,a new steam a- gent with high efficiency and its construction technology have been developed.By means of the cooperation of de- composed gas and surfactant,the oil displacement effi- ciency of non-homogeneity core increased by 16.5% on the average.With multi-slug injection and attached steam instilment,this technology has been used in Henan,Shengli and Kelamayi oilfield for more than 120 wells and total efficient rate has reached 92.5%.Field tests prove that the new agent has the advantages on in- creasing the formation energy,improving both the injec- ting steam conformance and oil displacement.It obviously enhances the production of stimulation wells,but fails in wells with high water cut(>85%)and serious steam channeling.
Keywords:heavy-oil thermal recovery  new technique  field trial  view
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