首页 | 本学科首页   官方微博 | 高级检索  
     

含硫气田天然气净化厂腐蚀控制与监/检测
引用本文:张强,黄刚华,江晶晶,熊钢,陈文.含硫气田天然气净化厂腐蚀控制与监/检测[J].石油与天然气化工,2018,47(2):19-25.
作者姓名:张强  黄刚华  江晶晶  熊钢  陈文
作者单位:中国石油西南油气田公司天然气研究院;国家能源高含硫气藏开采研发中心;中国石油天然气集团公司高含硫气藏开采先导试验基地
摘    要:川渝气田某天然气净化厂脱硫装置具有酸气负荷高、处理量大、胺液循环量大等特点,从检修结果看,再生塔底部、重沸器、半贫液返回线等位置腐蚀减薄严重。利用宏观观察、腐蚀挂片、氢探针等方法分析和评价了现场条件下的腐蚀状况,并制定了相应的腐蚀控制措施和监/检测方案。结果表明,循环量和酸气负荷较高是导致再生塔底部腐蚀严重的主要因素,碳钢内衬316L不锈钢可以较好地抑制再生塔底部环境下的腐蚀。

关 键 词:腐蚀  脱硫装置  H2S  胺液
收稿时间:2017/9/12 0:00:00

Corrosion control and monitoring/detection of natural gas purification plant in sour gas field
Zhang Qiang,Huang Ganghu,Jiang Jingjing,Xiong Gang and Chen Wen.Corrosion control and monitoring/detection of natural gas purification plant in sour gas field[J].Chemical Engineering of Oil and Gas,2018,47(2):19-25.
Authors:Zhang Qiang  Huang Ganghu  Jiang Jingjing  Xiong Gang and Chen Wen
Affiliation:Research Institute of Natural Gas Technology, PetroChina Southwest Oil and Gasfield Company, Chengdu, Sichuan, China;National Energy R&D Center of High Sulfur Gas Exploitation, Chengdu, Sichuan, China;High Sulfur Gas Exploitation Pilot Test Center, CNPC, Chengdu, Sichuan, China,Research Institute of Natural Gas Technology, PetroChina Southwest Oil and Gasfield Company, Chengdu, Sichuan, China;National Energy R&D Center of High Sulfur Gas Exploitation, Chengdu, Sichuan, China;High Sulfur Gas Exploitation Pilot Test Center, CNPC, Chengdu, Sichuan, China,Research Institute of Natural Gas Technology, PetroChina Southwest Oil and Gasfield Company, Chengdu, Sichuan, China;National Energy R&D Center of High Sulfur Gas Exploitation, Chengdu, Sichuan, China;High Sulfur Gas Exploitation Pilot Test Center, CNPC, Chengdu, Sichuan, China,Research Institute of Natural Gas Technology, PetroChina Southwest Oil and Gasfield Company, Chengdu, Sichuan, China;National Energy R&D Center of High Sulfur Gas Exploitation, Chengdu, Sichuan, China;High Sulfur Gas Exploitation Pilot Test Center, CNPC, Chengdu, Sichuan, China and Research Institute of Natural Gas Technology, PetroChina Southwest Oil and Gasfield Company, Chengdu, Sichuan, China;National Energy R&D Center of High Sulfur Gas Exploitation, Chengdu, Sichuan, China;High Sulfur Gas Exploitation Pilot Test Center, CNPC, Chengdu, Sichuan, China
Abstract:The desulfurization device of a natural gas purification plant in Sichuan-Chongqing gas field has the characteristics of high acid gas load, large processing capacity and amine circulation. The complete overhaul results showed that the corrosion thickness of the bottom of regenerator, reboiler, and the return line of semi-lean liquid were seriously decreased. The corrosion conditions in the field were analyzed and evaluated by macroscopic observation, corrosion coupon test and hydrogen probes, and the corresponding corrosion control measures and supervision/inspection schemes were developed. The results showed that the high cyclic volume and acid gas load were the main factors leading to the serious corrosion of the bottom of the regenerator, and the carbon steel inner lined 316L stainless steel could preferable inhibit the corrosion in the bottom of the regenerator.
Keywords:corrosion  desulphurization unit  H2S  amine solution
本文献已被 CNKI 等数据库收录!
点击此处可从《石油与天然气化工》浏览原始摘要信息
点击此处可从《石油与天然气化工》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号