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1.
The paper will report about the experiences at an Austrian large wastewater treatment plant of 720,000 population equivalents, where anaerobically digested sewage sludge is further stabilised under aerobic conditions. Enhanced stabilisation of the anaerobically digested sludge was required at the plant in order to get a permit for landfill disposal of the dewatered stabilized sludge. By implementing a post-aeration treatment (SRT approximately 6d; 36 degrees C) after anaerobic digestion the organic content of the anaerobically well digested sludge can be decreased by 16%. Investigations on site showed that during digested sludge post-aeration anoxic phases for denitrification are needed to provide stable process conditions. In this way the pH value can be kept in a more favourable range for micro-organisms and concrete structures. Additionally, inhibition of the biological process due to nitrite accumulation can be avoided. By optimising the aeration/pause ratio approximately 45% of total nitrogen in digested sludge can be removed. This significantly improves nitrogen removal efficiency at the wastewater treatment plant. NH(4)-removal occurs mainly through nitritation and denitritation with an efficiency of 98%. The costs/benefit analysis shows that post-aeration of digested sludge results in an increase of total annual costs for wastewater treatment of only 0.84%, corresponding to 0.19 Euro/pe/a. Result of molecular biological analyses (DGGE) indicate that all four ammonium-oxidizing bacteria species present in activated sludge can survive anaerobic digestion, but only two of them can adapt in the digested sludge post-aeration tanks. Additionally, in the post-aerated digested sludge a further ammonium-oxidizing bacteria species was identified.  相似文献   

2.
In wastewater treatment plants with anaerobic sludge digestion, 15-20% of the nitrogen load is recirculated to the main stream with the return liquors from dewatering. Separate treatment of this ammonium-rich digester supernatant significantly reduces the nitrogen load of the activated sludge system. Two biological applications are considered for nitrogen elimination: (i) classical autotrophic nitrification/heterotrophic denitrification and (ii) partial nitritation/autotrophic anaerobic ammonium oxidation (anammox). With both applications 85-90% nitrogen removal can be achieved, but there are considerable differences in terms of sustainability and costs. The final gaseous products for heterotrophic denitrification are generally not measured and are assumed to be nitrogen gas (N2). However, significant nitrous oxide (N2O) production can occur at elevated nitrite concentrations in the reactor. Denitrification via nitrite instead of nitrate has been promoted in recent years in order to reduce the oxygen and the organic carbon requirements. Obviously this "achievement" turns out to be rather disadvantageous from an overall environmental point of view. On the other hand no unfavorable intermediates are emitted during anaerobic ammonium oxidation. A cost estimate for both applications demonstrates that partial nitritation/anammox is also more economical than classical nitrification/denitrification. Therefore autotrophic nitrogen elimination should be used in future to treat ammonium-rich sludge liquors.  相似文献   

3.
Optimisation of nitrifying activated sludge plants towards nutrient removal (denitrification and enhanced P-removal) leads to a substantial reduction of operating costs and improves effluent and operating conditions. At WWTP Zürich-Werdh?elzli, initially designed for nitrification only, an anoxic zone of 28% of total activated sludge volume was installed and allowed 60% nitrogen elimination besides several other optimisations. In 2001 the operation of WWTP Zürich-Glatt was stopped and the wastewater was connected to WWTP Werdh?elzli. To improve nitrogen removal, WWTP Werdh?elzli co-financed two research projects; one for separate digester supernatant treatment with the anammox process operating two SBRs in series and the other applying NH4 sensors for aeration control in order to decrease energy consumption and raise effluent quality. The results of both projects and the consequences for WWTP Werdh?elzli are discussed in this paper.  相似文献   

4.
Traditional nitrification/denitrification is not suitable for nitrogen removal when wastewater contains high concentrations of ammonium nitrogen and low concentrations of biodegradable carbon. Recently, a deammonification process was developed and proposed as a new technology for treatment of such streams. This process relies on a stable interaction between aerobic bacteria Nitrosomonas, that accomplish partial nitritation and anaerobic bacteria Planctomycetales, which conduct the Anammox reaction. Simultaneous performance of these two processes can lead to a complete autotrophic nitrogen removal in one single reactor. The experiments where nitrogen was removed in one reactor were performed at a technical-scale moving-bed pilot plant, filled with Kaldnes rings and supplied with supernatant after dewatering of digested sludge. It was found that a nitrogen removal rate obtained at the pilot plant was 1.9 g m(-2) d(-1). Parallel to the pilot plant run, a series of batch tests were carried out under anoxic and aerobic conditions. Within the batch tests, where the pilot plant's conditions were simulated, removal rates reached up to 3 g N m(-2)d(-1). Moreover, the batch tests with inhibition of Nitrosomonas showed that only the Anammox bacteria (not anoxic removal by Nitrosomonas) are responsible for nitrogen removal.  相似文献   

5.
Fifty years ago when only BOD was removed at municipal WWTPs primary clarifiers were designed with 2-3 hours hydraulic retention time (HRT). This changed with the introduction of nitrogen removal in activated sludge treatment that needed more BOD for denitrification. The HRT of primary clarification was reduced to less than one hour for dry weather flow with the consequence that secondary sludge had to be separately thickened and biogas production was reduced. Only recently the ammonia rich digester liquid (15-20% of the inlet ammonia load) could be treated with the very economic autotrophic nitritation/anammox process requiring half of the aeration energy and no organic carbon source compared to nitrification and heterotrophic denitrification. With the introduction of this new innovative digester liquid treatment the situation reverts, allowing us to increase HRT of the primary clarifier to improve biogas production and reduce aeration energy for BOD removal and nitrification at similar overall N-removal.  相似文献   

6.
Nitrogen removal from organic wastewater is becoming a demand in developed communities. The use of nitrite as intermediate in the treatment of wastewater has been largely ignored, but is actually a relevant energy saving process compared to conventional nitrification/denitrification using nitrate as intermediate. Full-scale results and pilot-scale results using this process are presented. The process needs some additional process considerations and process control to be utilized. Especially under tropical conditions the nitritation process will round easily, and it must be expected that many AS treatment plants in the food industry already produce NO2-N. This uncontrolled nitrogen conversion can be the main cause for sludge bulking problems. It is expected that sludge bulking problems in many cases can be solved just by changing the process control in order to run a more consequent nitritation. Theoretically this process will decrease the oxygen consumption for oxidation by 25% and the use of carbon source for the reduction will be decreased by 40% compared to the conventional process.  相似文献   

7.
The Rya WWTP in Göteborg, Sweden is a highly loaded activated sludge plant which has been upgraded to remove nitrogen and to increase the biologically treated flow by 33% to reduce bypassing. Severe site restrictions made it difficult to increase the plant area. This was solved using a compact process based on tertiary nitrification in trickling filters and recirculation to a highly loaded activated sludge unit for denitrification. The necessary volumes were achieved by expanding the plant upwards, thus making it possible to place the trickling filters a in part of the area occupied by the former aeration basins. The recirculation of trickling filter effluent made it necessary to double the secondary settler capacity. This was solved by retrofitting the existing settlers as stacked settlers with a second tray on top of the original basin. The considerations behind process selection and plant design and costs are described.  相似文献   

8.
At a large Austrian municipal wastewater treatment plant enhanced stabilisation of anaerobically digested sewage sludge was required in order to get a permit for landfill disposal of the dewatered stabilized sludge. By implementing a post-aeration treatment after anaerobic digestion the organic content of the anaerobically well digested sludge can be decreased by 16%. Investigations at this plant showed that during digested sludge post-aeration anoxic phases are needed to provide stable process conditions. In this way the pH value can be kept in a more favourable range for micro-organisms and concrete structures. Additionally, under the process conditions applied nitrite accumulation would inhibit the stabilisation process if denitrification is not adequately applied. By optimising the aeration/pause ratio approximately 45% of total nitrogen in digested sludge can be removed. NH4-removal occurs through nitrification and denitrification with an efficiency of 98%. This significantly improves nitrogen removal efficiency at the wastewater treatment plant. The costs/benefit analysis shows that post-aeration of digested sludge results in an increase of total annual costs for wastewater treatment of only 0.84%, corresponding to 0.19 Euro/pe/a. Specific costs for nitrogen removal (0.32 Euro/kgN) are comparable with other biological processes for N-removal in reject water.  相似文献   

9.
The recycle water from sludge processing in municipal wastewater treatment plants causes many serious problems in the efficiency and stability of the mainstream process. Thus, the design approach for recycle water is an important part of any biological nutrient removal system design when a retrofit technology is required for upgrading an existing plant. Moreover, the application of nitrogen removal from recycle water using the nitritation process has recently increased due to economic reasons associated with an effective carbon allocation as well as the minimization of aeration costs. However, for the actual application of recycle water nitritation, it has not been fully examined whether or not additional volume would be required in an existing plant. In this paper, the addition of recycle water nitritation to an existing plant was evaluated based on a volume analysis and estimation of final effluent quality. It was expected that using the reserve volume of the aeration tank in existing plants, recycle water nitritation could be applied to a plant without any enlargement. With the addition of recycle water nitritation, it was estimated that the final effluent quality would be improved and stabilized, especially in the winter season.  相似文献   

10.
Nitrogen removal from sludge reject water was obtained by oxygen-limited partial nitritation resulting in nitrite accumulation in a first stage, followed by autotrophic denitrification of nitrite with ammonium as electron donor (similar to anaerobic ammonium oxidation) in a second stage. Two membrane-assisted bioreactors (MBRs) were used in series to operate with high sludge ages and subsequent high volumetric loading rates, achieving 1.45 kg N m(-3) day(-1) for the partial nitritation MBR and 1.1 kg N m(-3) day(-1) for the anaerobic ammonium oxidation MBR. Biomass retention in the nitritation stage ensured flexibility towards loading rate and operating temperature. Nitrite oxidisers were out-competed at low oxygen and high free ammonia concentration. Biomass retention in the second MBR prevented wash-out of the slowly growing bacteria. Nitrite and ammonium were converted to dinitrogen gas in a reaction ratio of 1.05, thereby maintaining nitrite limitation to assure process stability. The anoxic consortium catalysing the autotrophic denitrification process consisted of Nitrosomonas-like aerobic ammonium oxidizers and anaerobic ammonium oxidizing bacteria closely related to Kuenenia stuttgartiensis. The overall removal efficiency of the combined process was 82% of the incoming ammonium according to a total nitrogen removal rate of 0.55 kg N m(-3) day(-1), without adding extra carbon source.  相似文献   

11.
12.
Prague wastewater treatment plant was intensified during 1994--1997 by construction of new regeneration tank and four new secondary settling tanks. Nevertheless, more stringent effluent limits and operational problems gave rise to necessity for further intensification and optimisation of plant performance. This paper describes principal operational problems of the plant and shows solutions and achieved results that have lead to plant performance stabilisation. The following items are discussed: low nitrification capacity, nitrification bioaugmentation, activated sludge bulking, insufficient sludge disposal capacity, chemical precipitation of raw wastewater, simultaneous precipitation, sludge chlorination, installation of denitrification zones, sludge rising in secondary settling tanks due to denitrification, dosage of cationic polymeric organic flocculant to secondary settling tanks, thermophilic operation of digestors, surplus activated sludge pre-thickening, mathematical modelling.  相似文献   

13.
为了确认Biostyr曝气生物滤池工艺在中国的适应性,在高碑店污水处理厂进行了中试。记录和总结了2002年1月至2003年10月间的试验结果。取高碑店污水处理厂3系列初沉池出水为试验用水,试验期间水温在9-29℃。试验经历经典硝化/反硝化和同时硝化/反硝化的运行模式。以GB18918-2002为准,Biostyr滤池出水中化学耗氧量、总悬浮固体、氨基态氮、总氮等污染物均可达到其一级B标准。  相似文献   

14.
Development and implementation of a robust deammonification process.   总被引:4,自引:0,他引:4  
Deammonification represents a short-cut in the N-metabolism pathway and comprises 2 steps: about half the amount of ammonia is oxidised to nitrite and then residual ammonia and nitrite is anaerobically transformed to elementary nitrogen. Implementation of the pH-controlled DEMON process for deammonification of reject water in a single-sludge SBR system at the WWTP Strass (Austria) contributed essentially to energy self-sufficiency of the plant. The specific energy demand of the side-stream process equals 1.16 kWh per kg ammonia nitrogen removed comparing to about 6.5 kWh of mainstream treatment. Has this resource saving technology already approached state of the art? Deammonification has been operated in full-scale now for almost 3 years without interruption reaching annual ammonia removal rates beyond 90%. Biomass enrichment and DEMON-start-up in Strass took a period of 2.5 years whereas start-up period at the WWTP Glarnerland (Switzerland) was reduced to 50 days due to transfer of substantial amounts of seed sludge.  相似文献   

15.
New stricter nitrogen effluent standards and increasing influent loads require existing wastewater treatment plans (WWTPs) to extend or optimize. At WWTPs with limited aeration capacity, limited denitrification capacity or shortage of aerobic sludge age, implementation of SHARON to improve nitrogen effluent quality can be a solution. SHARON is a compact, sustainable and cost-effective biological process for treatment of nitrogen-rich rejection waters. At WWTP Rotterdam-Dokhaven and WWTP Utrecht a SHARON has been in operation for several years. For both WWTPs the effect of SHARON on the nitrogen effluent quality has been evaluated. WWTP Rotterdam-Dokhaven has limited aeration capacity. By implementation of SHARON, the ammonia load of the effluent was reduced by 50%. WWTP Utrecht had limited denitrification capacity. The implementation of SHARON improved the effluent nitrate load by 40%. The overall TN removal efficiency increased from 65% to over 75% and strict nitrogen effluents standards (TN = 10 mg N/l) could be reached. Through modelling and supported by full scale practice it has been shown that by implementation of SHARON in combination with enhanced influent pre-treatment, the aerobic sludge age can be extended to maintain total nitrogen removal at lower temperatures.  相似文献   

16.
In municipal WWTP with anaerobic sludge digestion, 10-20% of total nitrogen load comes from the return supernatant produced by the final sludge dewatering. In recent years a completely autotrophic nitrogen removal process based on Anammox biomass has been tested in a few European countries, in order to treat anaerobic supernatant and to increase the COD/N ratio in municipal wastewater. This work reports the experimental results of the SHARON-ANAMMOX process application to anaerobic supernatant taken from the urban Florentine area wastewater treatment plant (S. Colombano WWTP). A nitritation labscale chemostat (7.4 L) has been started-up seeded with the S. Colombano WWTP nitrifying activated sludge. During the experimental period, nitrite oxidising bacteria wash-out was steadily achieved with a retention time ranging from 1 to 1.5 d at 35 degrees C. The Anammox inoculum sludge was taken from a pilot plant at EAWAG (Zurich). Anammox biomass has been enriched at 33 degrees C with anaerobic supernatant diluted with sodium nitrite solution until reaching a maximum specific nitrogen removal rate of 0.065 kgN kg(-1) VSS d(-1), which was 11 times higher than the one found in inoculum sludge (0.005 kgN kg(-1) VSS d(-1). In a lab-scale SBR reactor (4 L), coupled with nitritation bioreactor, specific nitrogen removal rate (doubling time equal to 26 d at 35 degrees C and at nitrite-limiting condition) reached the value of 0.22 kgN kg(-1) VSS d(-1), which was approximately 44 times larger than the rate measured in the inoculum Anammox sludge.  相似文献   

17.
In wastewater treatment plants (WWTPs) equipped with sludge digestion and dewatering systems, the reject water originating from these facilities contributes significantly to the nitrogen load of the activated sludge tanks, to which it is typically recycled. In this paper, the impact of reject water streams on the performance of a WWTP is assessed in a simulation study, using the Benchmark Simulation Model no. 2 (BSM2), that includes the processes describing sludge treatment and in this way allows for plant-wide evaluation. Comparison of performance of a WWTP without reject water with a WWTP where reject water is recycled to the primary clarifier, i.e. the BSM2 plant, shows that the ammonium load of the influent to the primary clarifier is 28% higher in the case of reject water recycling. This results in violation of the effluent total nitrogen limit. In order to relieve the main wastewater treatment plant, reject water treatment with a combined SHARON-Anammox process seems a promising option. The simulation results indicate that significant improvements of the effluent quality of the main wastewater treatment plant can be realized. An economic evaluation of the different scenarios is performed using an Operating Cost Index (OCI).  相似文献   

18.
Boras wastewater treatment plant is being upgraded to comply with the new effluent standards for nitrogen. Three different configurations have been tested in parallel in full scale in the existing activated sludge plant The Biodenitro operated line showed the best performance because of the flexible adjustment of the nitrification and denitrification capacity. The adjustment was made off-line with the aid of continuous ammonia and nitrate measurements. On-line sensors are now installed permanently at Boris wastewater treatment plant and will be used for on-line dynamic control of the nitrogen removal in a Biodenitro configuration. The plant capacity will be further increased by Killing in the aeration tanks in situations with high hydraulic load.  相似文献   

19.
More stringent effluent criteria with regard to nitrogen calls for improved nutrient removal techniques in wastewater treatment plants (WWTPs). Besides optimisation of the liquid treatment train of the plants, attention has increasingly centred on the problem of return flows from sludge treatment. One of the most recent developments aimed at the reduction of this nitrogen load is deammonification which has been used at one of Ruhrverband's plants since 2002 by applying a moving bed system. To gain additional experience in operating this process, another full scale plant was modified in 2007 by integration of deammonification, using a SBR system with suspended biomass based on the DEMON(?) control scheme. By using seeding sludge from Strass WWTP in Austria, start-up has been achieved within only 1 day. After stable operation for several months, increasing nitrate concentrations were observed in the effluent of the system indicating growing activity of nitrite oxidising bacteria (NOB). Following severe process deterioration, it was decided to re-start the system again but the same behaviour, i.e. increasing levels of nitrate, was observed once again. Several approaches were used to suppress NOB organisms in full-scale without success, e.g. low oxygen levels and high free ammonia concentrations. Finally, the reduction of the aerobic cycle length during intermittent aeration down to 8 min, followed by an anoxic mixing period of only 18 min was successful in inhibiting the activity of NOB organisms, most probably due to their elevated lag-phase compared with ammonium oxidising bacteria. Today, nitrogen elimination that has been stabilised at more than 80% at a daily volumetric loading rate of 0.5 kg N/(m3 d). The total costs amount to €2.3/kg N(eli).  相似文献   

20.
Dewatering of digested sludge causes significant internal nitrogen loading to a wastewater treatment plant Due to the high concentration of nitrogen it is more effective to treat the reject-water not directly in the main purification process but to apply a separate biological treatment procedure. The intermittent operation of sludge-press facilities, the high initial pH-value of reject-water and the quick loss of alkalinity during nitrification makes a reliable control of the process necessary. A sequencing batch reactor (SBR) with an operational control based on on-line measurement of the pH-value is well suited to meet this requirement Such a control system for discontinuous treatment of reject-water has been extensively tested and optimised in full-scale experiments since 1995. The closed loop control of the pH-value was developed to keep the bicarbonate concentration within an optimum range. At the WWTP Strass in western Austria stable nitrification rates of 50 to 60 mg NH4-N/1/h have been achieved (elimination of 200 kg nitrogen per day).  相似文献   

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