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1.
在纺纱过程中,由于机械设备、纱线原料、加工工艺等不同,导致纱线质量参次不齐,质量问题会直接影响后道加工.纱线毛羽不仅影响织造还影响外观,针对如何更有效地去除织物表面的毛羽,提高成衣品质,改善服用性能,进行研究和试验,由正试验得出最佳工艺:清洗成衣—酵素食毛—亲水硅油柔软剂—桨翼式染缸内洗涤3 min—排水—加入聚丙烯酸...  相似文献   
2.
针对高精密加工过程中柔性夹具的变形问题进行理论计算和实验分析.首先应用CAE软件对现有柔性夹具进行有限元分析,分析夹具变形问题.然后通过CAD软件改变该夹具模型的结构参数和尺寸参数,优化夹具构造,以减少定位过程的夹具变形,并再次通过CAE软件进行分析,验证优化效果.通过增加夹具体主平面刚度、增加夹具体肋板刚度和改变夹具定位点位置等方法,实现夹具体的最大变形量满足加工精度的要求.实验分析以定位点变形为研究对象,测量得到4个定位点在夹具装夹过程中的变形量.实验结果基本符合理论计算结果,得到最终优化方案的4个定位点变形量均小于001 mm,满足了该高精密加工中对夹具体的精度要求.优化方案在实际生产中得到实施,效果良好.  相似文献   
3.
针对锦氨针织物难获得高色牢度的问题,采用锦纶助染剂DM-2250与酸性染料同浴染色,可提高色牢度与上染率。探讨了DM-2250用量和染色条件对锦纶上染率的影响。结果表明:当锦纶助染剂DM-2250质量分数为2.0%,锦纶染色不排液进行皂洗,上染率较传统工艺可提高6.7%,织物K/S值增加0.7左右,各项色牢度指标优于传统工艺染样0.5级,每次染色可节约用水2缸,节省染料约10%,省时约30 min。  相似文献   
4.
运用动态子结构固定界面模态综合法,结合Ansys有限元分析软件建立隧道-土层-建筑物系统动力学分析模型,通过与有限元整体建模分析法进行比较,验证了动态子结构法的准确性,对比分析系统的振动特性,分析隧道埋深、桩基深度对建筑物振动的影响。分析结果表明:隧道上方的建筑物桩基不利于建筑物减振,增加隧道埋深、增加隧道与建筑物桩尖的距离,可以有效降低建筑物振动。固定界面模态综合法具有较高的精度,计算效率高,在地铁列车引起建筑物振动分析中具有较好的适用性。  相似文献   
5.
为了研究低温空气等离子体在涤棉一浴法短流程染色生产中的应用,探讨等离子体作用时间、作用间距和放电电压对涤棉织物K/S值的影响。结果表明:等离子处理的优化工艺为作用时间5 min,作用间距2.5 mm,放电电压20 kV。经等离子处理后涤棉织物分散染料可以节省约27%,色牢度优于普通一浴法。  相似文献   
6.
由于二醋酸纤维耐热性差,目前这种面料做热转移数码印花比较少。研究了二醋酸纤维的软化点以及热转印机的热转印温度、转印速度和热压辊压力对数码印花效果的影响。结果表明,二醋酸纤维/阳离子染料可染改性涤纶热转移印花的优化工艺为:热转印温度190℃,热转印速度15 m/min,热压辊压力0.35 MPa,经过皂洗去除浮色,再加入聚醚型硅油柔软处理后,色牢度、透气性、吸湿性和舒适感更佳。  相似文献   
7.
为了染出仿牛仔效果,采用活性染料对毛衣进行染色。探究普通羊毛衫、丝光防缩羊毛衫染色过程中阳离子雅可固T24-C的用量、圆形橡胶浮球的用量,并对染色后羊毛衫的(K/S)值、(K/S反)值和正反面表观同色性K值进行评定。结果表明:丝光防缩羊毛衫反衫染色选用雅格素藏青BF-RRN 3.2%(omf),甲酸1.2%(omf),低温助剂ST220 1.5%(omf),雅可固T24-C 2.0%(omf),圆形橡胶浮球3.0%(omf)在85℃下运转15 min,随后用氨水在80℃下清洗6 min。羊毛衫正反面表观同色性K值为0.762,表明正反面色差大,且正面颜色比反面浅,羊毛衫有仿旧效果。  相似文献   
8.
In recent years, cotton fabrics, especially summer clothing, have been increasingly favored by young people in domestic market for their mercerization, moisture absorption, breathability and soft touch, and the market potential demanding for cotton cloth has been huge. Under the requirement of energy saving and emission reduction for high energy-consumption printing and dyeing enterprises by the Chinese government, most dyeing plants have adopted the more efficient short process of one-bath one-step cold pad-batch for cotton cloth bleaching. The hydrogen peroxide added in this process is over three times more than that of the traditional process. After oxygen bleaching mercerization of the cotton cloth, local excessive oxidation occurs and oxygen bleaching holes are more likely to occur. In the production process of cotton cloth, the selection process of different cotton cloth specifications is different resulting in complex reasons for holes. Therefore it is necessary to find out the causes of holes in the production process and formulate corresponding preventive measures and technological processes. In this experiment aldehyde cellulose produced by bleaching cotton cloth with hydrogen peroxide was oxidized by a self-made weak oxidation reagent so that metal silver atoms could be directly precipitated on the cloth surface. According to the number of silver atoms precipitated from the cloth surface and the hole opening the color depth was formed the intensity of hydrogen peroxide decomposition was judged and whether the hole on cotton cloth was caused by excessive oxidation was proved from the side. Then 1 mL of 8% silver nitrate solution and 2 mL of mixed solution of 20% sodium bicarbonate and 20% caustic soda were added into 17 mL of deionized water. Then the mixed solution was shaken up quickly. Subsequently 5g of cloth with holes was boiled in the solution for 2 min under 100 ℃ and then it was washed with deionized water. The color difference around the hole of that fabric was observed. The cotton cloth with holes were characterized by Fourier transform infrared spectroscopy X-ray diffraction scanning electron microscope SEM and X-ray photoelectron spectroscopy. The test results of the self-made solution show that the holes caused by mechanical and other external forces have the same color as the holes on the cloth surface indicating that the silver content precipitated is basically the same. As for holes caused by local overoxidation the color of the opening is darker than the cloth surface and the silver content of the hole area is obviously higher than that of other parts. During the test it is found that the decomposition rate of hydrogen peroxide is affected by temperatures pH values and metal ions and the symbionts and textile auxiliaries in gray cloth can inhibit the decomposition of hydrogen peroxide. Fourier transform infrared spectroscopy shows that the structure of most cotton fiber polysaccharides changes into dialdehyde cellulose after oxygen bleaching. After treatment with the self-made hole breaking detection reagent the aldehyde group and silver ions have oxidation-reduction reaction and the aldehyde group disappears. Through characterizing the cotton cloth tested by the self-made hole detection reagent it is concluded that the black particulate matters on the cotton cloth surface are silver atoms. The hole areas such as burnt holes hook holes weak yarn strength holes and damp mildew holes are of the same shade as the cloth surface. Nevertheless compared with the main elements of the cloth surface there are more black silver atoms in the hole than in other places which makes the color darker than in other places. As the demand for oxygen bleached mercerized cotton cloth is gradually increasing in domestic market it is significant to determine the causes of holes for production prevention which will be beneficial to cost saving and energy conservation and emission reduction. For the cotton cloth with holes during the production process the semi-finished cotton cloth can be treated through lower tension process on the machines increase the friction between yarns by adding adhesives or even be changed to the overflow or air cylinder with low tension for dyeing so as to reduce the probability of holes as much as possible and minimize the loss. In the future the weaving mill will equip the magnetic metal cloth inspection machine in the gray cloth inspection. As long as the fabric has more than a certain amount of metal ions the metal alarm device on the cloth inspection machine will raise the alarm to prevent the problematic gray cloth flowing into the next process which guarantees the good quality. © Journal of Silk.  相似文献   
9.
纬编针织物在生产过程中产生纬斜不可避免,特别是单面织物更加明显。使用黏合剂ST309 3.5%(omf),在压力为0.35 MPa、机速为15 m/min、140℃热压条件下使交联剂发生反应,黏合剂和交联剂呈立体网状薄膜,将毛羽固着在织物表面,能够增强纤维间的摩擦力,稳定纱线捻度,从而改善纬斜。经过处理后织物手感软滑,色牢度、顶破强力以及起毛起球性能都有所提升。  相似文献   
10.
羊毛衫的异味用传统方式很难去除干净,采用新型洗涤剂(含生物酶)能快速彻底去除异味,解决行业的老难题。去除异味的优化方案为:生物酶配比m(脂肪酶)∶m(蛋白酶)=1∶2,用量2%(omf),pH 5,温度450℃,时间30 min,此工艺处理毛衣的手感、颜色及洗净率均较好。  相似文献   
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