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多儿水电站泄水建筑物体型优化试验研究
引用本文:关文海,苗隆德,叶林,王波,朱兴华. 多儿水电站泄水建筑物体型优化试验研究[J]. 水资源与水工程学报, 2006, 17(2): 72-75
作者姓名:关文海  苗隆德  叶林  王波  朱兴华
作者单位:西安理工大学,水利水电学院,陕西,西安,710048
摘    要:通过水工模型试验研究,验证了多儿水电站泄水建筑物原设计方案的泄流能力、水面线分布等水力学技术指标。并采用复合曲线与扇形渠底局部抬高相结合的方法和渐变收缩挑流的消能方案优化了原设计方案中的溢洪道弯道段及出口段体型,有效地解决了由于水流冲击波引起的弯道水面高差过大以及尾水对对岸山体的冲刷影响的问题,并经过试验验证效果较好。以上研究成果为类似工程泄水建筑物的体型设计具有一定的借鉴意义。

关 键 词:弯道水流  建筑物体型优化  泄水建筑物  多儿水电站
文章编号:1672-643X(2006)02-0072-04
修稿时间:2005-08-03

Experiment research on form optimization of sluice structure of Duo''''er hydropower station
GUAN Wen-hai,MIAO Long-de,YE Lin,Wang Bo,ZHU Xing-hua. Experiment research on form optimization of sluice structure of Duo''''er hydropower station[J]. Journal of water resources and water engineering, 2006, 17(2): 72-75
Authors:GUAN Wen-hai  MIAO Long-de  YE Lin  Wang Bo  ZHU Xing-hua
Abstract:Through the hydraulic model tests of Duo'er hydropower station,many hydraulic technical indicators such as discharge capacity and water surface line distribution of sluice structures were given.Using compound curve combing with uplifting fan-shaped channel bottom and the contracted bucket dissipation projects to optimize the bend part and exit part of spillway in original design,this optimization solved the problem of the high water level amplitude because of the stream shock wave and the problem of tail water erode the mountain,were well validated by model tests.These results may present references for the optimized design of other flood-releasing works as well.
Keywords:bend flow  sluice structure form optimization  sluice structures  Duo'er hydropower station
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