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低渗透油藏微生物采油现场试验研究
引用本文:李蔚,刘如林,石梅,侯兆伟,韩培惠,杨振宇.低渗透油藏微生物采油现场试验研究[J].石油勘探与开发,2003,30(5):110-112.
作者姓名:李蔚  刘如林  石梅  侯兆伟  韩培惠  杨振宇
作者单位:1. 中国石油大庆油田勘探开发研究院
2. 南开大学生命科学院
基金项目:"九五"中国石油天然气集团公司攻关项目(961210609)
摘    要:大庆油田朝阳沟低渗透油藏是高黏度、高含蜡油葳,应用一系列生化分析的方法和手段,评价、监测在该油藏进行的微生物采油矿场试验的效果。试验结果,使用的种微生物在油层条件下都能较好存活,原油黏度的降低比率为43.7%/,含蜡量平均下降32.6%,含胶量平均下降31%,微生物产生的脂肪酸等活性物质降低了油水间的界面张力;气相色谱分析发现,原油中的正构烷烃碳数分布曲线向轻组分方向移动。矿场试验所取得的增油效果证实,利用微生物能提高低渗透油藏的原油采收率,增加原油产量,降低含水率,可能成为较好的增产调整措施之一。图3表5参11

关 键 词:大庆油田  低渗透油藏  微生物采油  混合菌种  现场试验
文章编号:1000-0747(2003)05-0110-03
修稿时间:2003年1月8日

Microbial enhanced oil recovery in low-permeability reservoir
LI Wei,LIU Rulin,SHI Mei,HOU Zhaowei,HAN Peihui and YANG Zhenyu.Microbial enhanced oil recovery in low-permeability reservoir[J].Petroleum Exploration and Development,2003,30(5):110-112.
Authors:LI Wei  LIU Rulin  SHI Mei  HOU Zhaowei  HAN Peihui and YANG Zhenyu
Affiliation:Exploration and Development Research Institute of Daqing Oilfield Company Ltd., Heilongjiang 163712, China;Nankai University, Tianjin 300071,China;Exploration and Development Research Institute of Daqing Oilfield Company Ltd., Heilongjiang 163712, China;Exploration and Development Research Institute of Daqing Oilfield Company Ltd., Heilongjiang 163712, China;Exploration and Development Research Institute of Daqing Oilfield Company Ltd., Heilongjiang 163712, China;Exploration and Development Research Institute of Daqing Oilfield Company Ltd., Heilongjiang 163712, China
Abstract:A huff-puff test with MEOR has been carried out in Chaoyanggou reservoir with a low permeability in Daqing Oilfield. By using a series of bio-chemical analyses, the evaluate and test on the effects of experiment and field show that the microbes can grow under the reservoir condition with low-permeability perfectly. The rheology of treated oil can be changed in a great deal and the content of paraffin and gel be reduced 31% and 32. 6%.respectively, due to the action of the bacteria. The interfacial tension between water and oil can be decreased. The gas chromatography analysis found that the light component increased and the heavy component decreased in crude oil. MEOR may be a good method to increase oil recovery and adjust wells for low-permeability layer with high viscous thinning oil.
Keywords:Daqing Oilfield  low-permeability reservoir  field test  MEOR  mixed bacteria
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