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SNCR烟气脱硝技术在330MW级CFB锅炉的应用
引用本文:韩应,高洪培,王海涛,李力,王润喜,宋晓刚.SNCR烟气脱硝技术在330MW级CFB锅炉的应用[J].洁净煤技术,2013(6):85-88.
作者姓名:韩应  高洪培  王海涛  李力  王润喜  宋晓刚
作者单位:[1]中国华能集团清洁能源技术研究院有限公司,北京100098 [2]华能白山煤矸石发电有限公司,吉林白山134700
摘    要:针对1180t/hCFB锅炉采用华能清能院选择性非催化还原(SNCR)脱硝专利技术,结合CFB锅炉炉内低NOx燃烧控制技术,NOx排放量由改造前的300mg/m3可有效控制在50mg/m3以下,脱硝效率达80%以上,对应氨氮比低于1.5,氨逃逸值可控制在1.5mg/m3以下,系统自动化投入率100%。通过对SNCR系统运行参数优化,得到较佳尿素给入浓度及合理的氨氮比控制参数,提高了脱硝系统的运行经济性、稳定性。该项技术首次成功应用于330MW等级CFB锅炉,为中国大型CFB锅炉实现高环保标准的氮氧化物减排探明了方向。

关 键 词:SNCR脱硝技术  循环流化床锅炉  氮氧化物  脱硝效率

Application of SNCR flue gas denitration technology in 330 MW CFB boiler
HAN Ying,GAO Hongpei,WANG Haitao,LI Li,WANG Runxi,SONG Xiaogang.Application of SNCR flue gas denitration technology in 330 MW CFB boiler[J].Clean Coal Technology,2013(6):85-88.
Authors:HAN Ying  GAO Hongpei  WANG Haitao  LI Li  WANG Runxi  SONG Xiaogang
Affiliation:2 ( 1. China Huaneng Clean Energy Research Institute ,Beijing 100098, China; 2. Huaneng Baishan Coal Gangue Power Generation Co. ,Ltd. , Baishan 134700, China)
Abstract:Owing to SNCR flue gas denitration technology and combustion control technology for CFB boiler, the NO~ concentration discharged by 1180 t/h CFB boiler decrease from 300 mg./m3 to less than 50 mg/m3. The denitration efficiency is above 80 percent, the ratio of ammonia to nitrogen is less than 1.5, ammonia escape value can be controlled under 1.5 mg/m3, automatic feeding rate is 100 percent. By optimizing operating parameters of SNCR system, get the optimum urea feeding concentration and ratio of ammonia to nitrogen, which guarantee the economy and stability of denitration system. This technology is first used in 330 MW CFB boiler, its operating experience provide reference for reducing NOx concentration discharged by CFB boiler.
Keywords:SNCR denitrification technology  CFB boiler  NOx  denitrification efficiency
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