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催化裂化汽油选择性加氢深度脱硫装置的试运行与改进
引用本文:庞少伟,付世昭,李栋.催化裂化汽油选择性加氢深度脱硫装置的试运行与改进[J].石化技术与应用,2011,29(1):53-57.
作者姓名:庞少伟  付世昭  李栋
作者单位:山东东明石化集团有限公司,山东,东明,274500
摘    要:介绍了山东东明石化集团有限公司100万t/a催化裂化汽油选择性加氢装置的试运行与改进情况。结果表明,预分馏塔在回流比为1.5~2.0,n(轻汽油馏分)/n(重汽油馏分)为55∶45条件下操作较好;平均加氢反应温度为285~290℃时重汽油馏分的脱硫率较高,烯烃饱和率较低,成品汽油的辛烷值损失较小;催化剂的选择因子只有1.55~1.69,显著低于实验室评价水平,对成品汽油的辛烷值损失影响较大,有待提高。

关 键 词:催化裂化汽油  选择性加氢  深度脱硫  辛烷值  OCT-MD技术

Trial operation and its improvement of deep selective hydrodesulfurization unit
Pang Shaowei,Fu Shizhao,Li Dong.Trial operation and its improvement of deep selective hydrodesulfurization unit[J].Petrochemical Technology & Application,2011,29(1):53-57.
Authors:Pang Shaowei  Fu Shizhao  Li Dong
Affiliation:Pang Shaowei,Fu Shizhao,Li Dong(Shandong Dongming Petrochemical Group Co Ltd,Dongming 274500,China)
Abstract:The trial operation and its improvement of deep selective hydrodesulfurization unit in Dongming Petrochemical Group Co Ltd were introduced.The results showed that the appropriate operating conditions for prefractionator were reflux ratio of 1.5-2.0 and mole ratio of low distillate gasoline to high distillate gasoline of 55 ︰ 45.The desulfurization percent was higher,the olefin saturation ratio was lower and the octane number loss was less for high distillate gasoline at average reaction temperature of 285-290℃.The catalyst selectivity index ranged only from 1.55 to 1.69,obviously lower than that of evaluation trial,and this would result in a larger loss in octane number and was expected to be improved in the future.
Keywords:catalytic cracking gasoline  selective hydrogenation  deep desulfurization  octane number  OCT-MD technology  
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