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不锈钢原料内在缺陷致冷轧断带的分析与改进
引用本文:燕顺,凌锐,唐振光,欧增微.不锈钢原料内在缺陷致冷轧断带的分析与改进[J].物理测试,2021,39(3):38-42.
作者姓名:燕顺  凌锐  唐振光  欧增微
作者单位:1. 广西北港新材料有限公司技术研究院,广西 北海 536000; 2. 广西北港新材料有限公司质量管理部,广西 北海 536000
摘    要:针对不锈钢原料内在缺陷导致的冷轧断带,采用扫描电子显微镜对断口形貌和成分进行分类,并对异物轧入、夹杂物和脆断的影响因素进行了探讨.结果表明,需根据断口不同的微观形貌和成分特征去制定改进措施.通过精炼工序适当延长软吹镇静时间可以减少辅料及炉衬耐材夹渣;通过连铸工序稳定拉速、改善冷却、优化结晶器流场及加强结晶器液面监控可以...

关 键 词:不锈钢  冷轧断带  微观形貌  夹杂物
收稿时间:2020-07-21

Analysis and improvement of cold rolling strip breaking caused by internal defects of stainless steel raw materials
YAN Shun,LING Rui,TANG Zhenguang,OU Zengwei.Analysis and improvement of cold rolling strip breaking caused by internal defects of stainless steel raw materials[J].Physics Examination and Testing,2021,39(3):38-42.
Authors:YAN Shun  LING Rui  TANG Zhenguang  OU Zengwei
Affiliation:1.Technical Research Institute, Guangxi BG New Co., Ltd., Beihai 536000, China; 2.Quality Management Department, Materials Co., Ltd., Beihai 536000, China
Abstract:In view of the strip breaking during cold rolling caused by internal defects of stainless steel raw materials, the morphology and composition of the fracture surface were analyzed by scanning electron microscopy (SEM). Moreover, the influencing factors of rolled in extraneous material, inclusions and brittle fracture were discussed. The results showed that the improvement measures should be made according to the different micro morphology and composition characteristics of the fracture. The slag inclusion of auxiliary materials and lining refractory could be reduced by prolonging the soft blowing and sedation time properly in refining process. The slag entrapment could be reduced and the slab quality could be improved by stabilizing casting speed, improving the cooling condition, optimizing the mold flow field, and strengthening the monitoring of mold liquid level in continuous casting process. The rolled in coatings residual could be eliminated by adjusting the marking code size and position of slabs. The risk of cold rolled brittle fracture could be decreased by finely tuning the steel chemical composition and reducing the thickness of raw materials. After the implementation of improvement measures above, the frequency of strip breaking during cold rolling caused by internal defects of stainless steel raw materials reduced by more than 70% compared with before.
Keywords:stainless steel  cold rolling strip breaking  micro morphology  inclusion  
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