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丰满大坝整体性研究综述
引用本文:宋恩来.丰满大坝整体性研究综述[J].大坝与安全,2002(3):15-19.
作者姓名:宋恩来
作者单位:国家电力公司东北公司,沈阳,110006
摘    要:丰满大坝纵缝上部未设键槽,蓄水前又未灌浆;水平施工缝结合不好,坝体还有各种裂缝,对整体性有一定的影响。丰满大坝于1987年开始进行了全面的加固,整体性得到改善和加强。丰满电厂委托多家进行整体性研究分析,本文介绍各分析成果,并进行综合分析。

关 键 词:丰满大坝  纵缝  施工缝  裂缝  整体  性大坝安全
文章编号:1671-1092(2002)03-0015-05
修稿时间:2001年1月15日

Summary on integrity study for Fengman Dam
by Song Enlai//Northeast Company of SPCC.Summary on integrity study for Fengman Dam[J].Large Dam & Safety,2002(3):15-19.
Authors:by Song Enlai//Northeast Company of SPCC
Affiliation:by Song Enlai//Northeast Company of SPCC
Abstract:There are no key-ways made in the upper longitudinal joints in Fengman Dam and no grouting before impounding.Poor bind-ing in horizontal joints,a variety of cracks are existed in dam body.All those will have a certain effect on its integrity.Fengman Dam has been reinforced comprehensively since1987,1so its integrity has improved and strengthened.Many companies have been charged to study its integrity.This paper introduced the all results from different companies and made an integrated analysis on it.
Keywords:Fengman Dam  longitudinal joint  construction joint  crack  integrity  dam safety  
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