首页 | 本学科首页   官方微博 | 高级检索  
     

抽油井泵效分析
引用本文:曾亚勤.抽油井泵效分析[J].石油天然气学报,1999,21(1):42-44,47.
作者姓名:曾亚勤
作者单位:长庆石油勘探局第一采油厂,陕西,延安,717405
摘    要:考虑自由气,含气液体的体积收缩,漏失,油管和抽油杆的弹性伸缩等4个方面的影响,对C油田H区块抽油井的泵效进行了理论计算。结果表明,实际泵效明显低于理论值,其主要原因是凡尔漏失或堵塞以及油管严重结蜡或结盐。

关 键 词:抽油井  泵效  沉没度  尾管
文章编号:1000-9752(1999)01-0042-03

Evaluating Pump Efficiency of Pumping Wells
ZENG Ya-qing.Evaluating Pump Efficiency of Pumping Wells[J].Journal of Oil and Gas Technology,1999,21(1):42-44,47.
Authors:ZENG Ya-qing
Abstract:A theoretical analysis for pump efficiency of pumping wells in the block H of the field C is made in consideration of 4 effects such as free gas, shrinkage and leakage of gaseous liquid, and elastic elongation and shrinkage of tubing and sucker rod. The analysis results show that the real value of pump efficiency is apparently lower than its theoretical value because of a leakage or blockage of valves and severe plugging of paraffins and scales. The analysis also shows that the submergence depth of the most wells in the block is not reasonable Its correct value should be: the submergence depth is 350-450m while water cut<0 6 and 300-400m while water cut=0 6-0 9 as well as 200-300m while water cut>0 9. It is suggested that the current submergence depth should be modified to eliminate incorrect location of liners.
Keywords:pumping well  pump efficiency  submergence depth  liner  
本文献已被 CNKI 维普 万方数据 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号