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龙开口水电站冲沙底孔泄槽段掺气设施试验研究
引用本文:徐曼,王均星,陈规划. 龙开口水电站冲沙底孔泄槽段掺气设施试验研究[J]. 水电能源科学, 2011, 29(4)
作者姓名:徐曼  王均星  陈规划
作者单位:1. 武汉大学水资源与水电工程科学国家重点实验室,湖北武汉,430072
2. 水利部珠江水利委员会珠江水利综合技术中心,广东广州,510610
摘    要:以龙开口水电站冲沙底孔泄槽段为例,针对常规掺气设施不能确保掺气效果问题,基于原设计方案提出了2个优化方案,并通过水工模型进行了试验和比较分析,确定了较合理的掺气设施。结果表明,有压出口底部采用突跌掺气并加设挑坎,泄槽段采用坎槽结合式的掺气形式,掺气减蚀效果较好。

关 键 词:泄槽段  平坡  掺气设施  突跌  空腔  龙开口水电站  

Experimental Research on Aerator of Chute Section of Sand Flush Bottom Outlet for Longkaikou Hydropower Station
XU Man,WANG Junxing,CHEN Guihua. Experimental Research on Aerator of Chute Section of Sand Flush Bottom Outlet for Longkaikou Hydropower Station[J]. International Journal Hydroelectric Energy, 2011, 29(4)
Authors:XU Man  WANG Junxing  CHEN Guihua
Affiliation:XU Man1,WANG Junxing1,CHEN Guihua2 (1.State Key Laboratory of Water Resources and Hydropower Engineering Science,Wuhan University,Wuhan 430072,China,2.Pearl River Water Conservancy Commission Integrated Technology Center,Guangzhou 510610,China)
Abstract:The conventional aerating facilities can not ensure the aeration effect.Taking chute section of sand flush bottom outlet of Longkaikou Hydropower Station for an example,this paper proposes two optimized programs based on the original design scheme.The reasonable aerating facilities are determined with hydraulic model test.Results show that the program can produce a good cavitation reduction effect,which adopts the combination of sudden bottom drop for aeration and flip bucket in outlet of pressured spillway...
Keywords:chute section  flat slope  aerating facilities  sudden bottom drop  cavity  Longkaikou Hydropower Station  
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