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气举作业中连续油管腐蚀断裂原因
引用本文:郑华安,闫化云,佟琳,谢思宇,李飞. 气举作业中连续油管腐蚀断裂原因[J]. 腐蚀与防护, 2011, 0(9): 758-760
作者姓名:郑华安  闫化云  佟琳  谢思宇  李飞
作者单位:中海石油(中国)有限公司湛江分公司;中海油能源发展股份有限公司上海采油技术服务分公司;西安摩尔石油工程实验室;
摘    要:某海上气井连续氮气气举作业61.5h后,发生连续油管断裂,观察发现连续油管外壁腐蚀严重。通过宏观和微观分析、理化性能检验、X射线衍射和模拟试验,对腐蚀油管进行了失效分析。结果表明,气举作业所用氮气携带的O2和井内CO2共同作用造成了连续油管腐蚀破坏,氧腐蚀是造成短时间内连续油管严重腐蚀的主要因素。针对此结论和现场工况,...

关 键 词:氮气气举  连续油管  氧腐蚀  二氧化碳腐蚀

Corrosion Cracking Cause of Coiled Tubing in Gas Lift Operation
ZHENG Hua-an,YAN Hua-yun,TONG Lin,XIE Si-yu,LI Fei. Corrosion Cracking Cause of Coiled Tubing in Gas Lift Operation[J]. Corrosion & Protection, 2011, 0(9): 758-760
Authors:ZHENG Hua-an  YAN Hua-yun  TONG Lin  XIE Si-yu  LI Fei
Affiliation:ZHENG Hua-an~1,YAN Hua-yun~2,TONG Lin~3,XIE Si-yu~1,LI Fei~2 (1.Zhanjiang Branch of CNOOC Ltd.,Zhanjiang 524057,China,2.CNOOC Energy Technology & Services Shanghai Oilfield Technology Services Branch,Shanghai 200000,3.Xi'an Maurer Petroleum Engineering Laboratory,Xi'an 710065,China)
Abstract:A coiled tubing in an offshore gas well cracked and suffered serious corrosion after nitrogen gas-lift operation for 61.5 h.The failure cause of the tubing was studied by macro and micro analysis,physical and chemical properties testing,X-ray energy spectrum analysis and stimulated corrosion test.The results showed that the combined effect of O_2 carried by N_2 and CO_2 in the wet gas well corroded the coiled tubing.The O_2 corrosion was the main reason of the corrosion of coiled tubing in short time.Accord...
Keywords:nitrogen gas-lift  coiled tubing  O_2 corrosion  CO_2 corrosion  
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