首页 | 本学科首页   官方微博 | 高级检索  
     

天然气浅冷装置冷量回收优化工艺
引用本文:吴新阳.天然气浅冷装置冷量回收优化工艺[J].石油炼制与化工,2010,41(5):62-65.
作者姓名:吴新阳
作者单位:大庆油田有限责任公司天然气分公司,大庆,163318
摘    要:以大庆油田有限责任公司天然气分公司浅冷装置为例,分析浅冷装置轻烃和外输干气冷量回收现状,提出存在的问题及改进措施。在通过HYSIM软件进行模拟计算的基础上,对各种改造方案进行分析和比较,最终提出采用多股流换热器的冷量回收工艺。在浅冷装置上采用该优化工艺时,按轻烃和外输干气回收温度达到10℃计,回收热量263.6MJ/h,富天然气温度由5℃降到-1.94℃,氨蒸发器的负荷降低20.4%,年节电6.061×105kWh,年节约生产成本47.7万元。

关 键 词:天然气  浅冷装置  冷量回收  多股流换热器  优化
收稿时间:2009-10-22

PROCESS OPTIMIZATION FOR RECOVERING COLD ENERGY OF NATURAL GAS SHALLOW CONDENSING UNIT
Wu Xinyang.PROCESS OPTIMIZATION FOR RECOVERING COLD ENERGY OF NATURAL GAS SHALLOW CONDENSING UNIT[J].Petroleum Processing and Petrochemicals,2010,41(5):62-65.
Authors:Wu Xinyang
Abstract:Taking the shallow condensing unit of Daqing Oilfield Natural Gas Company as an example, the current cold energy recovery situation of light hydrocarbon and export dry gas of shallow condensing unit was analyzed. Some existed problems and measures of improvement were put forward. Various schemes for improvement were compared based on the simulation computations by HYSIM software. Finally, a cold energy recovery process using multi-flow heat exchanger was proposed. After adopting said optimized process, when the recovery temperature of light hydrocarbon and export dry gas was 10℃, 263.6 MJ/h of cold energy could be recovered, the temperature of rich natural gas was decreased to -1.94℃ from 5℃, the load of ammonia evaporator reduced by 20.4%, the annual saving of electricity and production cost reached 60.61×104 kWh and 0.477 MRMB, respectively.
Keywords:natural gas  shallow condensing unit  cold engergy recovery  multi-flow heat exchanger  optimization
本文献已被 CNKI 万方数据 等数据库收录!
点击此处可从《石油炼制与化工》浏览原始摘要信息
点击此处可从《石油炼制与化工》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号