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三板溪面板堆石坝渗流监测资料分析
引用本文:李涛,王玉洁,朱锦杰.三板溪面板堆石坝渗流监测资料分析[J].大坝与安全,2009(6).
作者姓名:李涛  王玉洁  朱锦杰
作者单位:国家电力监管委员会大坝安全监察中心,浙江,杭州,310014
摘    要:三板溪面板堆石坝最大坝高185.5 m,蓄水初期水库在低水位运行,总渗漏量基本在30 L/s以下,2007年汛期库水位迅速抬高,总渗漏量突然增大,最大达303.10 L/s。后经水下检查,发现在面板一、二期水平缝部位出现多处破损并进行了修复,面板修复取得了一定的效果。本文结合渗流监测资料重点对面板破损前后大坝渗流性态进行了分析。

关 键 词:三板溪面板堆石坝  渗漏量  面板破损

Analysis on the seepage monitoring data of Sanbanxi face-slab rock-fill dam
LI Tao,WANG Yu-jie,ZHU Jin-jie.Analysis on the seepage monitoring data of Sanbanxi face-slab rock-fill dam[J].Large Dam & Safety,2009(6).
Authors:LI Tao  WANG Yu-jie  ZHU Jin-jie
Affiliation:LI Tao; WANG Yu-jie and ZHU Jin-jie Large Dam Safety Supervision Center of SERC;
Abstract:The height of Sanbanxi face-slab rock-fill dam is 185.5 m.With low storage water level,the seepage was less than 30 L/s.As water level rising rapidly in the flood season of 2007,the seepage increased,whose maximum was 303.10 L/s.By underwater in-spection,damage was found at the horizontal joints of the face-slab.Later,rehabilitation was carried out and good effect was gotten.This paper,combined with seepage monitoring data,analysed the seepage of the dam before and after the rehabilitation.
Keywords:Sanbanxi face-slab rock-fill dam  seepage  damage of face slab  
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