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贵广二回高压直流逆变站无通信紧急跳闸试验的仿真分析
引用本文:饶宏,蔡希鹏,傅闯,李岩.贵广二回高压直流逆变站无通信紧急跳闸试验的仿真分析[J].南方电网技术,2007,1(2):13-18.
作者姓名:饶宏  蔡希鹏  傅闯  李岩
作者单位:1. 南方电网技术研究中心,广东,广州,510623
2. 南方电网超高压输电公司,广东,广州,510623
摘    要:贵广二回极2于2007年5月29日进行了小功率(150 MW)无通信逆变站手动紧急跳闸试验。试验方案预期,在试验工况下,在逆变站按下紧急停机(ESOF)按钮后,整流站将在1 s后由直流低电压保护(27DC)启动闭锁顺序。但实际试验结果显示,整流站由换流器过压保护59/37DC一段启动紧急停机顺序,退回至备用状态。本文对这种异常情况进行了分析,并对分析结论做了PSCAD/EMTDC仿真验证。根据分析建议的试验方案进行的再次试验证明了分析的正确性。

关 键 词:贵广二回直流工程  系统调试  紧急停机顺序  PSCAD/EMTDC
收稿时间:8/3/2007 12:00:00 AM

Simulation Analysis on the Abnormal Results of the Manual ESOF Test to Gui-Guang II HVDC Link System
RAO Hong,CAI Xi-peng,FU Chuang and LI Yan.Simulation Analysis on the Abnormal Results of the Manual ESOF Test to Gui-Guang II HVDC Link System[J].Southern Power System Technology,2007,1(2):13-18.
Authors:RAO Hong  CAI Xi-peng  FU Chuang and LI Yan
Affiliation:CSG Technology Research Center;CSG EHV Power Transmission Company;CSG Technology Research Center;CSG Technology Research Center
Abstract:The low load (150 MW) manual emergency switch off (ESOF) trip test at inverter station without telecommunication of Guizhou-Guangdong II HVDC project Pole 2 was carried out on May 29, 2007. It is expected by the test project that in this situation the rectifier station will be blocked by the DC undervoltage protection (27DC) after the ESOF button is initiated at the inverter station. However, it was actually tripped in the test by the converter overvoltage protection (59/37DC). Analysis on this abnormal results and the PSCAD/EMTDC simulation are addressed. A new test scheme based on this study has been implemented to verify our conclusion.
Keywords:Gui-Guang II HVDC project  system test  emergency switch off sequence (ESOF)  PSCAD/ EMTDC
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