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UR T35/T60变压器差动保护误动分析
引用本文:方愉冬,杨涛,吴春娣. UR T35/T60变压器差动保护误动分析[J]. 电力系统保护与控制, 2009, 37(14)
作者姓名:方愉冬  杨涛  吴春娣
作者单位:1. 浙江电力调度通信中心,浙江,杭州,310007
2. 浙江电力试验研究院,浙江,杭州,310004
3. 镇海发电厂,宁波,镇海,315208
摘    要:针对某电厂T35/T60变压器差动保护误动,对保护数据波形和整定值进行了分析.根据波形特征理论分析,排除了和应涌流引起差动保护误动的可能,指出系穿越性励磁涌流的非周期分量导致CT暂态饱和,从而引起采用"2-out-of-3"谐波制动方式的差动保护误动.最后针对误动事故,提出了T35/T60保护二次谐波制动方式选择和差动动作曲线整定上应采取的措施.

关 键 词:主变差动保护  励磁涌流  CT暂态饱和  误动

Analysis on mal-operation of UR T35/T60 transformer differential protection
FANG Yu-dong,YANG Tao,WU Chun-di. Analysis on mal-operation of UR T35/T60 transformer differential protection[J]. Power System Protection and Control, 2009, 37(14)
Authors:FANG Yu-dong  YANG Tao  WU Chun-di
Abstract:The paper analyzes fault data and protection setting during a mal-operation of UR T35/T60 transformer differential protection relay.Based on theoretical analysis of waveform character, possibility of sympathetic inrush resulting in mal-operation is ruled out, and conclusion is drawn that mal-operation was caused by differential protection's "2-out-of-3" 2nd harmonic restraint mode and TA transient saturation due to through-by inrush current.The corresponding solution of mal-operation is proposed on T35/T60 relay percent differential operating characteristic setting and 2nd harmonic restraint choice.
Keywords:transformer differential protection  inrush current  CT transient saturation  mal-operation
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