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水处理残渣调剖剂室内研究及现场应用
引用本文:Hou Tianjiang,Zhao Huating,Li Zongtian,Zhao Puchun,Xiao Liping. 水处理残渣调剖剂室内研究及现场应用[J]. 石油科学(英文版), 2005, 2(4): 50-55
作者姓名:Hou Tianjiang  Zhao Huating  Li Zongtian  Zhao Puchun  Xiao Liping
作者单位:Petroleum Engineering Department of Zhongyuan Petroleum Exploration Bureau,SINOPEC,Puyang,Henan 730001,China,The Third Production Factory,Zhongyuan Petroleum Exploration Bureau,SINOPEC,Shenxian,Shandong 252435,China,Petroleum Engineering Department of Zhongyuan Petroleum Exploration Bureau,SINOPEC,Puyang,Henan 730001,China,The Third Production Factory,Zhongyuan Petroleum Exploration Bureau,SINOPEC,Shenxian,Shandong 252435,China,The Third Production Factory,Zhongyuan Petroleum Exploration Bureau,SINOPEC,Shenxian,Shandong 252435,China
摘    要:1. Introduction Zhongyuan Oilfield is a complex oilfield with many small fault blocks. Since it entered the high water-cut production period, secondary large porous channels have created, making it difficult to perform profile control and water plugging (…

关 键 词:水处理  溢流  油田  多孔渗水  堵漏处理
收稿时间:2004-11-29
修稿时间:2004-11-29

Study of Water Treatment Residue Used as a Profile Control Agent
Hou Tianjiang,Zhao Huating,Li Zongtian,Zhao Puchun and Xiao Liping. Study of Water Treatment Residue Used as a Profile Control Agent[J]. Petroleum Science, 2005, 2(4): 50-55
Authors:Hou Tianjiang  Zhao Huating  Li Zongtian  Zhao Puchun  Xiao Liping
Affiliation:1. Petroleum Engineering Department of Zhongyuan Petroleum Exploration Bureau, SINOPEC,Puyang, Henan 730001, China
2. The Third Production Factory, Zhongyuan Petroleum Exploration Bureau, SINOPEC,Shenxian, Shandong 252435, China
Abstract:A large amount of residue from the water treatment process has gradually accumulated and thus caused serious environmental pollution in waterflood oilfields. The water treatment residue is a grey suspension, with a density of 1.08 g/cm3, and mainly contains over 65% of light CaCO3, MgCO3, CaSO4, Fe2S3 and Ca(OH)2. This paper ascertains the effect of water treatment residue on core permeability and its application in oilfields. Coreflooding tests in laboratory were conducted in two artificial cores and one natural core. Core changes were evaluated by cast model image analysis, mercury injection method and scanning electron microscopy (SEM). Fresh water was injected into another natural core, which was plugged with water treatment residue, to determine the effective life.The results indicate that the water treatment residue has a strongly plugging capability, a resistance to erosion and a long effective life, and thus it can be used as a cheap raw material for profile control.In the past 8 years, a total of 60,164 m3 of water treatment residue has been used for profile control of 151 well treatments, with a success ratio of 98% and an effective ratio of 83.2%. In the field tests, the profile control agent increased both starting pressure and injection pressure of injectors, and decreased the apparent water injectivity coefficient, significantly improving intake profiles and lengthening average service life of injectors. 28,381 tons of additional oil were recovered from these corresponding oil wells, with economic benefits of ¥3,069.55×104 (RMB) and a remarkable input-output ratio of 8.6:1.
Keywords:Water treatment residue   coreflooding test   profile control agent   permeability modification   field application
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