首页 | 本学科首页   官方微博 | 高级检索  
     

湖北某铜尾矿资源化利用研究
引用本文:杨伟卫,蔡恒安,尚世超,毛益林.湖北某铜尾矿资源化利用研究[J].金属矿山,2022,51(5):135-141.
作者姓名:杨伟卫  蔡恒安  尚世超  毛益林
作者单位:1.湖北省地质局第一地质大队,湖北 大冶 435000;2.中国地质科学院矿产综合利用研究所,四川 成都 610041;3.中国地质调查局金属矿产资源综合利用技术研究中心,四川 成都 610041
摘    要:湖北某铜尾矿中有价组分为WO3、Cu、S、Fe,为实现该铜尾矿的资源化利用,开展了详细的综合回收试验研究。结果表明:① 采用铜硫混合浮选、铜硫混合精矿再磨后铜硫分离浮选工艺流程处理试样,闭路试验可获得产率0.10%、Cu品位13.80%、Cu回收率21.71%的铜精矿以及产率1.22%、S品位44.50%、S回收率50.89%的硫精矿。② 采用2粗2扫1精常温浮选处理铜硫混浮尾矿,常温精矿浓缩至60%,再加温至90 ℃,搅拌、解吸80 min后采用1粗2扫5精加温精选、中矿顺序返回的工艺流程,最终获得产率0.93%、WO3品位15.31%、WO3回收率55.07%的钨精矿产品;该钨精矿进行酸浸提质,最终获得产率0.40%、WO3品位34.19%、WO3回收率53.04%的酸浸钨精矿。③ 针对钨粗选尾矿,采用弱磁选工艺可获得产率3.73%、TFe品位60.45%、回收率15.66%的铁精矿。

关 键 词:铜尾矿  白钨矿  铜硫分离  加温精选  

Research on Resource Utilization of a Copper Tailing in Hubei
YANG Weiwei,CAI Heng'an,SHANG Shichao,MAO Yilin.Research on Resource Utilization of a Copper Tailing in Hubei[J].Metal Mine,2022,51(5):135-141.
Authors:YANG Weiwei  CAI Heng'an  SHANG Shichao  MAO Yilin
Affiliation:1.The First Geological Brigade of Hubei Geological Bureau,Daye 435000,China; 2.Institute of Multipurpose Utilization of Mineral Resource,CAGS,Chengdu 610041,China; 3.Research Center of Multipurpose Utilization of Metal Mineral Resources of China Geological Survey,Chengdu 610041,China
Abstract:In order to realize the resource utilization of a copper tailings in Hubei,a detailed experimental study on comprehensive recovery was carried out.The results showed that:① The copper concentrate with yield of 0.10%,Cu grade of 13.80% and Cu recovery rate of 21.71% and the sulfur concentrate with yield of 1.22%,S grade of 44.50% and S recovery rate of 50.89% could be obtained in closed circuit test by using copper sulfur mixed flotation and copper sulfur separation flotation process after regrinding of copper sulfur mixed concentrate.② Two roughing,two scavenging and one cleaning were used to treat copper sulfur mixed floating tailings by flotation at room temperature.Next,the room temperature concentrate was concentrated to the concentration of 60%,then heated to 90 ℃,stirred and desorbed for 80 min,followed by one roughing,two scavenging and five cleaning for heating cleaning,middling back in sequence.Finally,the tungsten concentrate with yield of 0.93%,WO3 grade of 15.31% and WO3 recovery rate of 55.07% was obtained.The tungsten concentrate quality was improved by acid leaching.Finally,an acid leaching tungsten concentrate with yield of 0.40%,WO3 grade of 34.19% and WO3 recovery rate of 53.04% was obtained.③ For tungsten roughing tailings,iron concentrate with yield of 3.73%,TFe grade of 60.45% and recovery rate of 15.66% could be obtained by low intensity magnetic separation process.
Keywords:
本文献已被 万方数据 等数据库收录!
点击此处可从《金属矿山》浏览原始摘要信息
点击此处可从《金属矿山》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号