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芳烃联合装置氢气压缩机组凝汽器的在线清洗
引用本文:林辉. 芳烃联合装置氢气压缩机组凝汽器的在线清洗[J]. 石油化工, 2002, 31(11): 925-927
作者姓名:林辉
作者单位:天津石油化工公司,设备管理处,天津,300271
摘    要:芳烃联合装置凝汽器的结垢是氢气压缩机负荷降低的主要原因。在线清洗凝汽器是较佳的解决方案,通过采用10%氨基磺酸和缓蚀剂等添加剂,控制清洗温度为50~65℃,在降低氢气压缩机负荷后,对凝汽器进行一侧清洗,一侧运行。在线清洗后,凝汽器换热效果及真空度都达到最好水平,氢气压缩机恢复正常生产负荷。

关 键 词:氢气压缩机  汽轮机  凝汽器  清洗  清洗剂
文章编号:1000-8144(2002)11-0925-03
修稿时间:2002-04-20

On-Line Purge of Steam Condenser of Hydrogen Compressor in Aromatic Complex Unit
LIN Hui. On-Line Purge of Steam Condenser of Hydrogen Compressor in Aromatic Complex Unit[J]. Petrochemical Technology, 2002, 31(11): 925-927
Authors:LIN Hui
Abstract:In an aromatic complex unit ,the main cause for decrease in hydrogen compressor load was scale formation in steam condenser.A good solution was on-line purge of the steam condenser.After decreasing the load ,the steam condenser was purged on one side using 10% sulfamic acid and corrosion inhibitor at 50~60 ℃ with the other side still running.After purging,the best heat exchanger effect and vacuum pressure could be obtained and the load of hydrogen compressor returned to normal value.
Keywords:hydrogen compressor  steam turbine  steam condenser  purge  detergent
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