首页 | 本学科首页   官方微博 | 高级检索  
     

油田热采注汽系统软化污水结垢原因
引用本文:冯庆伟,温涛,温建萍.油田热采注汽系统软化污水结垢原因[J].石油化工腐蚀与防护,2004,21(4):45-47.
作者姓名:冯庆伟  温涛  温建萍
作者单位:1. 中国石化股份有限公司胜利油田分公司,山东,东营,257068
2. 南京航空航天大学材料科学与技术学院,江苏,南京,210016
摘    要:中国石化股分有限公司胜利油田分公司现河采油厂乐安油田热采注汽系统于 2 0 0 0年 2月使用软化污水以后 ,在炉管、蒸汽输送管线、井下工具等部位发生了结垢 (结盐 ) ,造成 30 1号湿蒸汽发生器爆管事故。X -射线衍射、能谱元素分析表明 :污水中二氧化硅及钾、钠离子超标 (SiO2 含量 5 0mg/L ,Na+ +K+ 含量2 4 4 4 .7mg/L)导致在高温加热条件下生成硅酸盐沉积是上述部位结垢的根本原因 ,而注汽系统及井下管柱泄漏引起温度、压力改变导致了结垢的发生。建议应对泄漏部位及时维修并研制相应的高温抗垢剂。

关 键 词:蒸汽发生器  注汽系统  结垢  高温抗垢剂
文章编号:1007-015X(2004)04-0045-03
修稿时间:2003年12月17

Fouling of Demineralized Waste Water in Steam Inject system of Oil Field
Feng Qingwei,Wen Tao.Fouling of Demineralized Waste Water in Steam Inject system of Oil Field[J].Petrochemical Corrosion and Protection,2004,21(4):45-47.
Authors:Feng Qingwei  Wen Tao
Abstract:When the demineralized waste water was used for the steam injection system in the oil field in Shengli Oil Field Co., Ltd/SINOPEC in February, 2000, fouling (salt deposit) occurred in the furnace tubes, steam pipelines and well tools etc, which led to tube fracture of 301 wet steam generator. The x-ray and energy spectrum analysis show that the basis cause of the fouling is the deposit of silicate formed in high temperature conditions due to the excessive SiO_2, Na+ and K+ (SiO_2: 50 mg/L, Na+ and K+ : 2444.7 mg/L). The temperature and pressure changes caused by the leakage of well pipe and steam injection system results in the fouling. It is recommended that a timely maintenance on the leakage location be made and high-temperature anti-fouling agent be developed.
Keywords:steam generator  steam injection system  fouling  high-temperature anti-fouling agent
本文献已被 CNKI 维普 万方数据 等数据库收录!
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号