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高拱坝深基坑渗流控制措施及分析
引用本文:陆马兰.高拱坝深基坑渗流控制措施及分析[J].长江科学院院报,2009,26(Z1).
作者姓名:陆马兰
作者单位:中国水电顾问集团公司,成都勘测设计研究院坝工处,成都,610072
摘    要:在建溪洛渡高拱坝施工过程中,通过对河床深基坑出现涌水的成因分析,采取了减渗帷幕封闭渗水、截排地表水、降水等施工措施,达到控制河床深基坑涌水的目的.通过其效果分析,提出减渗帷幕的厚度和减渗帷幕深入相对隔水层最小深度,应当满足渗流稳定的要求;对强透水性基岩,要确定好幕体的防渗标准,即幕体的渗透系数与岩体渗透系数的比值,其值不大于0.1 ,渗透流量就明显减少;对先期导水通道灌浆封堵并进行坝基固结灌浆,不仅是坝体地基加固的需要,同时也是施工期加强基坑底部抵抗承压水能力的需要.

关 键 词:深基坑  渗流稳定  渗流控制  涌水  减渗帷幕灌浆  固结灌浆  减渗效率  承压水

Seepage Control Measures and Analysis for Deep Foundation Pit of High Arch Dam
LU Ma-lan.Seepage Control Measures and Analysis for Deep Foundation Pit of High Arch Dam[J].Journal of Yangtze River Scientific Research Institute,2009,26(Z1).
Authors:LU Ma-lan
Affiliation:LU Ma-lan (Institute of CHECC-Dam Design Department,Chengdu Hydropower Investigation Design & Research,Chengdu 610072,China)
Abstract:During construction of Xiludu High Arch Dam,the cause analysis on water blowing out from deep foundation pit in the riverbed was performed,the construction measures,such as sealing infiltration water with antiseepage curtain,intercepting and draining the surface water,pumping and draining the water in the pit,were taken in order to control the water blowing out from deep pit.In this paper,thickness of seepage reducing curtain and the minimum depth into relative impermeable layer,which should meet seepage st...
Keywords:deep foundation pit  seepage stability  seepage control  water burst  seepage reducing curtain grouting  consolidation grouting  seepage reducing efficiency  confined water  
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