首页 | 本学科首页   官方微博 | 高级检索  
     

塔河油田稠油有杆泵井杆断裂研究与治理对策
引用本文:袁波, 涂东, 杜林辉, 蒋磊, 王磊磊. 塔河油田稠油有杆泵井杆断裂研究与治理对策[J]. 石油实验地质, 2014, 36(s1): 135-138. doi: 10.11781/sysydz2014S1135
作者姓名:袁波  涂东  杜林辉  蒋磊  王磊磊
作者单位:中国石化 西北油田分公司 塔河采油二厂, 新疆轮台 841604
摘    要:通过对塔河油田采油二厂杆断裂情况、监测的功图载荷及杆柱应力评价、注气及断杆腐蚀情况、断杆前的生产异常情况的综合分析,结合送检断裂杆的失效分析报告,认为抽油杆断裂主要影响因素是高负载、高交变载荷下的疲劳断裂以及注气及硫化氢腐蚀;通过进一步分析认为:泵型的合理选择、泵深的合理确定、杆柱设计的优化、严格的生产管控及抽油杆的合理优选可以有效地降低抽油杆断裂几率.

关 键 词:抽油杆   交变载荷   疲劳断裂   塔河油田
收稿时间:2014-10-08
修稿时间:2014-11-20

Research of fractured sucker rod in heavy oil of Tahe Oilfield and countermeasures
Yuan Bo, Tu Dong, Du Linhui, Jiang Lei, Wang Leilei. Research of fractured sucker rod in heavy oil of Tahe Oilfield and countermeasures[J]. PETROLEUM GEOLOGY & EXPERIMENT, 2014, 36(s1): 135-138. doi: 10.11781/sysydz2014S1135
Authors:Yuan Bo  Tu Dong  Du Linhui  Jiang Lei  Wang Leilei
Affiliation:Tahe No.2 Oil Production Plant, SINOPEC Northwest Company, Luntai, Xinjiang 841604, China
Abstract:Through the comprehensive analyses of the rod fracture situation, the diagram of load monitoring, the rod stress evaluation, the fractured sucker rod corrosion and the abnormal situation before broken, combined with the failure analysis report of fractured rod, the main influencing factors of sucker rod fracture mainly include high load, high alternating load and corrosion of hydrogen sulfide and injection gas. The reasonable choice of pump and pump depth, the optimization of rod string design, the strict production control and the reasonable optimization of pumping rod can effectively reduce the probability of sucker rod fracture.
Keywords:sucker rod  alternating load  fatigue fracture  Tahe Oilfield
点击此处可从《石油实验地质》浏览原始摘要信息
点击此处可从《石油实验地质》下载全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号