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提高水平井φ77.8mm尾管固井质量的措施
引用本文:赵凤森,贾晓斌.提高水平井φ77.8mm尾管固井质量的措施[J].石油钻采工艺,2002,24(6):18-20.
作者姓名:赵凤森  贾晓斌
作者单位:1.中国石化新星公司西北分公司工程监理中心, 新疆塔里木 842017
摘    要:塔河油田的水平井产量优势明显。但水平井φ177.8mm尾管的固井质量差,严重影响了油田的评价与开发。在TC423、TH105、TH106、TH107、TH1085口井当中,仅TH106井的声幅测井合格。为适应今后生产发展的需要,工程监理中心对水平井φ177.8mm尾管固井作了专题研究,通过室内试验优选出可有效驱替含油钻井液的水泥浆配方,选择性能可靠的井下工具与合适的施工参数,制定出保证套管下到位的措施。通过6口井的试验,1次固井合格率达到100%,其中优质率50%。

关 键 词:塔河油田    水平井    尾管    固井质量
收稿时间:2019-05-22
修稿时间:2002年9月3日

Improving the φ177.8mm Liner Cementing Quality in Horizontal Well
Affiliation:1.Engineering Supervision Center of the Northwest Branch of New Star Company, SINOPEC, Tarim, Xinjiang
Abstract:well enhances the production greatly in Tahe Oilfield, while due to the poor cementing quality of the φ177.8mm liner in horizontal wells, the evaluation and development work is negatively influenced.In the cemented five wells, the acoustic amplitude logging of only one well was up to standard.To solve this problem, monographic study on φ177.8mm liner cementing was conducted by the Engineering Supervision Center.Cement slurry system of effective oil-containing drilling fluid displacement efficiency was optimized by laboratory tests, and reliable downhole tools were selected with suitable operating parameters;measures for ensuring the proper casing setting location were also planed.Tests in 6 wells were very successful, the cementing quality of all the wells was up to standard and half of wells achieved excellent quality.
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