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天广直流系统双极线路保护误动作分析
引用本文:田庆.天广直流系统双极线路保护误动作分析[J].南方电网技术,2011,5(5):26-29.
作者姓名:田庆
作者单位:中国南方电网超高压输电公司检修试验中心,广州,510663
摘    要:天广直流线路自主化改造后8个月内保护共动作了22次,其中3次为双极线路保护同时动作。对这3次双极线路保护误动作进行了分析,结合厂家给出的突变量保护定值和整定思想,进行了2项整改:降低低电压保护定值和增大突变量保护的动作延时。整改后至今未再发生双极线路保护同时动作情况。

关 键 词:天广直流输电线路  突变量保护  双极线路  保护动作
收稿时间:5/9/2011 12:00:00 AM

Analysis on the Fault Trip of Bipolar DC Line Protection in Tianshengqiao-Guangzhou HVDC System
QING Tian.Analysis on the Fault Trip of Bipolar DC Line Protection in Tianshengqiao-Guangzhou HVDC System[J].Southern Power System Technology,2011,5(5):26-29.
Authors:QING Tian
Affiliation:Test and Maintenance Center, CSG EHV Power Transmission Company, Guangzhou 510663, China
Abstract:8 months after control and protection modification completed in Tianshengqiao-Guangzhou HVDC System, line protection has tripped 22 times. 3 of these are bipolar line protection false tripping, which are analyzed in this paper. Two corresponding methods: lowing the under voltage protection value and increasing the du/dt protection value, are put forward according to the protection threshold values and the setting process given by the manufacturers. No bipolar line protection accident occurs until now with the above methods implemented.
Keywords:Tianshengqiao-Guangzhou HVDC Transmission Line  du/dt protection  bipolar DC line  protection trip  
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