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新型方钢管混凝土梁柱节点抗震性能研究
引用本文:王先铁,郝际平,孙彤,潘阳,任青青,马山积,李娜.新型方钢管混凝土梁柱节点抗震性能研究[J].土木与环境工程学报,2007,29(2):73-77.
作者姓名:王先铁  郝际平  孙彤  潘阳  任青青  马山积  李娜
作者单位:1. 西安建筑科技大学,西建大-莱钢钢结构研发中心,陕西西安,710055
2. 山东莱钢建设有限公司,山东青岛,266071
摘    要:通过低周反复加载试验对3个内隔板一面贯通式节点进行了试验研究,研究了不同轴压比情况下节点的滞回性能、强度及刚度退化、延性、耗能性能及破坏特征。试验结果表明,试件的层间位移延性系数为2.11~2.32,峰值荷载时的能量耗散系数为1.141~1.502。提出了抗震设计、研究建议。

关 键 词:方钢管混凝土柱  梁柱节点  内隔板贯通  试验研究  抗震性能
文章编号:1006-7329(2007)02-0073-05
修稿时间:2006-12-27

Experimental Study on Seismic Behavior of Penetrated Interior Diaphragm on One Side Beam-to-Column Connection for Concrete-Filled Square Steel Tube
WANG Xian-tie,HAO Ji-ping,SUN Tong,PAN Yang,REN Qing-qing,MA Shan-ji,LI Na.Experimental Study on Seismic Behavior of Penetrated Interior Diaphragm on One Side Beam-to-Column Connection for Concrete-Filled Square Steel Tube[J].Journal of Civil and Environmental Engineering,2007,29(2):73-77.
Authors:WANG Xian-tie  HAO Ji-ping  SUN Tong  PAN Yang  REN Qing-qing  MA Shan-ji  LI Na
Abstract:A total of three experimental specimens of penetrated interior diaphragm on one side had been tested under low-cyclic reversed loading to study the hysteric behavior,strength and stiffness degradation,ductility,energy dissipation capacity and the failure modes.The only difference of all specimens was the axial compression ratio.Experimental results show that the story drift ductility ratios are 2.11~2.32,and the energy dissipation ratios are 1.141~1.502 at the peak load.Additional anti-seismic design and research recommendations are presented.
Keywords:concrete-filled steel square tubular column  beam-to-column connection  through interior diaphragm  experimental study  seismic behavior
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