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胜三区抽油杆失效机理分析及措施研究
引用本文:卢建平,刘文业,董志东,张桂意,邵红钰. 胜三区抽油杆失效机理分析及措施研究[J]. 断块油气田, 2001, 8(6): 60-62
作者姓名:卢建平  刘文业  董志东  张桂意  邵红钰
作者单位:胜利油田有限公司胜利采油厂
摘    要:胜三区抽油杆断脱成为有杆泵失效的主要因素,抽油杆的失效大大加重了油井的维护费用。对此,主要从矿场生产的角度,对胜三区抽油杆失效的化学因素和物理因素进行深入细致的分析。在现场采取了加缓蚀剂、简化管柱、控制油井沉没度、降低含砂量和应用防偏磨工艺等措施,取得了较好效果。

关 键 词:抽油杆 胜利油田 失效机理 化学因素 物理因素
修稿时间:2001-09-06

Analysis and Treatment on Failure Mechanism of Rod In Block 3 of Shengtuo Oilfield
Lu Jianping. Analysis and Treatment on Failure Mechanism of Rod In Block 3 of Shengtuo Oilfield[J]. Fault-Block Oil & Gas Field, 2001, 8(6): 60-62
Authors:Lu Jianping
Abstract:In the light of breaking of sucker rods being the main failure factors of rod pumping wells in block 3 of Shengtuo Oilfield, which increase the well' s maintenance cost, this paper deeply analysis the chemical and physical failure factors, through the aspects of field production. Some technical measure having been put into use, obvious results are obtained.
Keywords:Sucker rod   Failure factor    Measure  
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