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A /O泳动床反应器脱氮性能研究
引用本文:谈玲玲,张岩,郭岩,小山登一郎,张杰.A /O泳动床反应器脱氮性能研究[J].给水排水,2009,35(Z1).
作者姓名:谈玲玲  张岩  郭岩  小山登一郎  张杰
作者单位:1. 北京工业大学北京市水质科学与水环境恢复工程重点实验室,北京,100124
2. NET株式会社,日本,666-0115
基金项目:北京市教育委员会科技发展计划面上项目,中日合作研究与开发项目 
摘    要:基于A/O工艺与泳动床工艺技术的联合,开发出A/O泳动床生物膜反应器.A/O泳动床系统表现出高效去除COD_(Cr)、NH_3-N和TN以及较好的抗负荷冲击能力.在HRT=12.5 h,回流比为300%,进水COD_(Cr)、NH_3-N平均浓度分别为343.4 mg/L、94.1 mg/L时,COD_(Cr)和NH3-N平均去除率分别为84.6%, 86.8%;COD_(Cr)的容积负荷与去除负荷现良好的线性关系,R~2=0.970 4;系统在较低的C/N下,TN平均去除率为70.8%.

关 键 词:A/O泳动床  脱氮

STUDY ON NITROGEN REMOVAL BY A/O SWIMMING BED REACTEOR
Tan Lingling,Zhang Yan,Guo Yan,Koyama Nobuichiro,Zhang Jie.STUDY ON NITROGEN REMOVAL BY A/O SWIMMING BED REACTEOR[J].Water & Wastewater Engineering,2009,35(Z1).
Authors:Tan Lingling  Zhang Yan  Guo Yan  Koyama Nobuichiro  Zhang Jie
Abstract:Anoxic/oxic(A/O) process combined with swimming bed as a novel technology for wasterwater treatment was developed, which was on the basis of A/O process and swimming bed technology.The results demonstrated that A/O swimming bed system has the performance of high-efficiency removal of COD_(Cr)、NH_3-N and TN, as well as resistant to flash loading.When hydraulic retention times (HRT) was at 12.5 h with average concentration of influent wasterwater's COD_(Cr) and NH_3-N of 343.4 mg/L、94.1 mg/L,the average COD_(Cr) and NH_3-N removal rate of 84.6% and 86.8% were achieved separately.Linearity relationship was appeared between volumetric loading and removal loading, R~2=0.970 4;70.8% of average remaoval rate were achieved in lower ratio of C/N.
Keywords:HRT  A/O swimming bed  Removal nitrogen  HRT
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