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苏4-14井借气气举排水采气技术
引用本文:高贵民,朱世民,刘东,崔金榜,李向齐,马凤芹,孙卫华.苏4-14井借气气举排水采气技术[J].石油钻采工艺,2006,28(4):44-45,49.
作者姓名:高贵民  朱世民  刘东  崔金榜  李向齐  马凤芹  孙卫华
作者单位:1.华北油田公司第四采油厂, 河北 廊坊 065007
摘    要:针对深度达到4825 m的苏4-14气井开采中产出液体影响气井生产的问题,借用邻井高压气实施气举排水采气工艺措施,排出井底积液,建立生产压差,恢复气井生产。该井自2005年8月开始气举并恢复生产,到2006年4月增产天然气1.37×107m3,累计采油2.0114×103t。该技术具有投资少、施工周期短的特点,对今后类似气井的复产具有重要的指导意义。

关 键 词:天然气    凝析气藏    深层    大产水量    气井    气举    排水采气
文章编号:1000-7393(2006)04-0044-02
收稿时间:2006-04-27
修稿时间:2006-04-27

Gas-lift dewatering technology of Su 4-14 by using gas from adjacent wells
GAO Gui-min,ZHU Shi-min,LIU Dong,CUI Jin-bang,LI Xiang-qi,MA Feng-qin,SUN Wei-hua.Gas-lift dewatering technology of Su 4-14 by using gas from adjacent wells[J].Oil Drilling & Production Technology,2006,28(4):44-45,49.
Authors:GAO Gui-min  ZHU Shi-min  LIU Dong  CUI Jin-bang  LI Xiang-qi  MA Feng-qin  SUN Wei-hua
Affiliation:1.Huabei Oilfield Fourth Oil Factory, Langfang 065007, Hebei, China
Abstract:Su 4-14 is a deep gas well with a depth of 4825 m.The output of liquid decreased gas Production greatly.A technical measure was carried out to load the liquid in the wellbore and re-establish production difference,by using gas from adjacent high-pressure gas well.The production of Su 4-14 was resumed after the gas-lift dewatering measure in August,2005,and 1.37×107m3 natural gas and(2.0114)×103 t oil were increased by April,2006.This technology has the characteristics of low-investment and short construction period,which could be popularized to the production restoration of similar gas wells.
Keywords:natural gas  condensate gas reservoir  deep reservoir  water production  gas well  gas-lifting  dewatering gas recovery  
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