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深厚软土地区某厂房基础沉降原因分析和对策
引用本文:丁国雄,谯伟.深厚软土地区某厂房基础沉降原因分析和对策[J].探矿工程(岩土钻掘工程),2007,34(5):8-11.
作者姓名:丁国雄  谯伟
作者单位:1. 宁波市江北城市工业投资开发有限公司,浙江,宁波,315000
2. 浙江省岩土基础公司,浙江,宁波,315040
摘    要:某厂房由于软土排水固结和地面回填堆载产生地面沉降过大,针对各部位荷载与地质条件的不同情况,分别采用了袖阀管静压注浆和锚杆静压桩托换技术对软土地基进行加固处理,取得了良好效果。介绍了袖阀管静压注浆法和锚杆静压桩托换法的技术特点、加固机理及施工工艺。

关 键 词:软土地基  地基沉降  袖阀管注浆  锚杆静压桩  基础托换
文章编号:1672-7428(2007)05-0008-04
修稿时间:2006-08-252006-12-26

Analysis on Cause of Workshop Foundation Subsidence in Deep Thick Soft Ground Area and the Countermeasure
DING Guo-xiong,QIAO Wei.Analysis on Cause of Workshop Foundation Subsidence in Deep Thick Soft Ground Area and the Countermeasure[J].Exploration Engineering:Rock & Soil Drilling and Tunneling,2007,34(5):8-11.
Authors:DING Guo-xiong  QIAO Wei
Affiliation:1. Ningbo Jiangbei City Industrial Investment Develops Co. , Ltd, Ningbo Zhejiang 315000, China; 2. Zhejiang Geo-foundation Company, Ningbo Zhejiang 315040, China
Abstract:Excessive land subsidence occurred because of drainage consolidation and backfill loading for soft clay foundation of a workshop, static pressure grouting with sleeve valve pipe and anchor static pressure pile underpinning technique were adopted to consolidate the soft ground foundation, and the technical features, consolidation mechanism and construction technology were introduced in this paper.
Keywords:soft clay foundation  foundation subsidence  grouting with sleeve valve pipe  anchor static pressure pile  foundation underpinning
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