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某集气管线穿孔失效原因分析
引用本文:吴华,毛汀,霍绍全,蒋志.某集气管线穿孔失效原因分析[J].石油与天然气化工,2022,51(6):104-108.
作者姓名:吴华  毛汀  霍绍全  蒋志
作者单位:中国石油西南油气田公司天然气研究院;中国石油西南油气田公司川中油气矿
摘    要:目的 确定四川某集气管线腐蚀穿孔的原因。方法 采用直读光谱仪、金相显微镜、X-射线衍射仪和扫描电镜及EDS能谱对失效样品进行检测,并对腐蚀环境进行了分析。结果 (1)管体内壁存在大量腐蚀凹坑,管体金相组织为铁素体+珠光体,焊缝组织为针状铁素体,管基体的冶金质量、化学成分和力学性能符合标准;(2)腐蚀产物为FeS和少量FeCO3;(3)气田水中存在硫酸盐还原菌(SRB)。结论 管线穿孔是SRB、H2S、CO2等因素共同作用的结果。

关 键 词:穿孔  集气管线  腐蚀  失效分析
收稿时间:2021/11/28 0:00:00

Cause analysis of perforation failure of a gas gathering pipeline
Wu Hu,Mao Ting,Huo Shaoquan,Jiang Zhi.Cause analysis of perforation failure of a gas gathering pipeline[J].Chemical Engineering of Oil and Gas,2022,51(6):104-108.
Authors:Wu Hu  Mao Ting  Huo Shaoquan  Jiang Zhi
Affiliation:Research Institute of Natural Gas Technology, PetroChina Southwest Oil & Gasfield Company, Chengdu, Sichuan, China; Central Sichuan Oil and Gas District, PetroChina Southwest Oil & Gasfield Company, Suining, Sichuan, China
Abstract:ObjectiveThe perforated corrosion sample of a natural gas gathering pipeline in Sichuan was studied to determine its failure reason. Methods The failure samples were tested by direct-reading spectrometer, optical microscope, X-ray diffractometer, scanning electron microscope and EDS, and the corrosion condition was analyzed. Results(1) A large number of corrosion pits can be seen on the inner surface of the pipeline. The matrix of the pipeline was ferrite plus pearlite, and the weld seam was acicular ferrite. Its metallurgical quality, chemical composition and mechanical properties meet the national standard requirements.(2) The corrosion products were FeS and FeCO3.(3) SRB existed in the gas field water. ConclusionsThe cause of pipeline perforation is the result of SRB, H2S, CO2 and other factors.
Keywords:perforation  gas gathering pipeline  corrosion  failure analysis
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