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克拉玛依油田八区下乌尔禾组油藏小井距开发试验
引用本文:覃建华,丁艺,阳旭,池建萍,潘前樱,路培毅,林革. 克拉玛依油田八区下乌尔禾组油藏小井距开发试验[J]. 新疆石油地质, 2009, 30(6): 725-727
作者姓名:覃建华  丁艺  阳旭  池建萍  潘前樱  路培毅  林革
作者单位:1.中国石油大学 资源与信息学院,北京 102249; 2.中国石油 新疆油田分公司 勘探开发研究院,新疆 克拉玛依 834000; 3.中国石油 西部钻探公司 测井公司研究所,新疆 克拉玛依 834000; 4.中国石油 西部钻探公司 国际事业部,乌鲁木齐 830000
摘    要:克拉玛依油田八区下乌尔禾组油藏为巨厚的特低渗透砾岩油藏,前期采用 275 m 井距反九点井网注水开发,油井见效低、压力保持程度低、采油速度低,低渗透储集层较大注采井距难以建立有效水驱是开发效果差的主要原因。小井距试验通过细分开发层系、缩小井距、改变井网方式以建立有效水驱体系。将开发层系细分为 3 套,逐层上返,首先试验 P2w4 ,由 275 m×388 m 反九点井网加密为 138 m×195 m 反九点井网,后期转为五点井网平行裂缝方向注水。同时,控制单井注水量,采用点弱面强的注采政策。试验 3 a 后,与八区正常井距区块相比,各项开发指标明显好转,预计可提高采收率 8.5%.

关 键 词:克拉玛依油田  砾岩油藏  特低渗透油藏  小井距试验  加密井  开发层系  
收稿时间:2009-03-17

Pilot Test of Close Spacing Development in Lower Wuerhe Reservoir of District No.8 of Karamay Field
QIN Jian-hua,DING Yi,YANG Xu,CHI Jian-ping,PAN Qian-ying,LU Pei-yi,LIN Ge. Pilot Test of Close Spacing Development in Lower Wuerhe Reservoir of District No.8 of Karamay Field[J]. Xinjiang Petroleum Geology, 2009, 30(6): 725-727
Authors:QIN Jian-hua  DING Yi  YANG Xu  CHI Jian-ping  PAN Qian-ying  LU Pei-yi  LIN Ge
Affiliation:1. Faculty of Natural Resource and Information Technology, China University of Petroleum, Beijing 102249, China; 2. Research Institute of Exploration and Development, Xinjiang Oilfield Company, PetroChina, Karamay, Xinjiang 834000, China; 3. Institute of Well Logging Company, West Drilling Company, PetroChina, Karamay, Xinjiang 834000, China; 4. International Department, West Drilling Company,PetroChina, Urumqi, Xinjiang 830000, China
Abstract:Lower Wuerhe reservoir of District No.8 in Karamay oil field is a thick massive ultra-low permeability conglomerate reservoir,and was developed by waterflooding process with inverted nine-spot pattern and well spacing of 275 m in one series of strata in early stage.But it featured such poor development effects as the low efficiency of response for producers,low pressure maintenance degree and low oil production rate.The low permeability reservoir and larger producer-injector well spacing should be the main reasons for it was hard to establish effective waterflood response.This paper presents the close spacing pilot test that is to establish effective waterflood system by subdividing the layer series of development,decreasing the well spacing and changing the well patterns.The layer series of development is subdivided into three layers and recompleted layer by layer.The WU-4 unit is the first layer to be tested.The inverted nine-spot well pattern is infilled from 275 m×388 m to 138 m×195 m in the first stage and then converted into five-spot pattern to take a waterflood along parallel fractures,while controlling the injection flow rate by strategy of water drive weak at the spot and intensive in the area.Three-year test has shown that the production indices are all better than the original ones before,and it is expected that the recovery factor will be increased by 8.5%by this test.
Keywords:Karamay field  conglomerate reservoir  low permeability  close spacing test  infill well  layer series of development
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