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甲基叔丁基醚裂解制异丁烯装置的操作优化
引用本文:杨志毅,周天基,宋晓轩. 甲基叔丁基醚裂解制异丁烯装置的操作优化[J]. 石化技术与应用, 2007, 25(2): 156-159
作者姓名:杨志毅  周天基  宋晓轩
作者单位:中国石油兰州石油化工公司红叶公司,甘肃兰州,730060;中国石油兰州石化分公司炼油厂,甘肃兰州,730060
摘    要:通过改进甲基叔丁基醚(MTBE)裂解制异丁烯(IB)装置甲醇脱水塔控制方案和优化催化剂活化温度、活化时间、通风量以及反应温度等操作条件,使该装置由原设计的“一反六塔”流程改进为“一反三塔”流程,甲醇收率由30.08%提高到33.47%,异丁烯收率由54.01%提高到58.14%,装置能耗由8648.76 MJ/t降低至5 863.15 MJ/t。

关 键 词:甲基叔丁基醚  裂解  异丁烯  工业装置  操作优化
文章编号:1009-0045(2007)02-0156-04
修稿时间:2006-08-182006-09-20

Operation optimum for isobutene production by methyl-tert-butyl ether cracking
Yang Zhiyi,Zhou Tianji,Song Xiaoxuan. Operation optimum for isobutene production by methyl-tert-butyl ether cracking[J]. Petrochemical Technology & Application, 2007, 25(2): 156-159
Authors:Yang Zhiyi  Zhou Tianji  Song Xiaoxuan
Abstract:The control program of methanol dewatering tower was improved,and the catalyst activating conditions such as temperature,time and air quantity as well as reactive temperature were optimized.Based on above works,the process flow of isobutene production by methyl tert-butyl ether cracking was changed from one-reactor-six-tower to one-reactor-three-tower system.The results showed that the methanol yield increased from 30.08% to 33.47%,the isobutene yield increased from 54.01% to 58.14%,and the engery consumption of the device reduced from 8648.76MJ/t to 5863.15MJ/t.
Keywords:methyl-tert-butyl ether  cracking  isobutene  industrial device  operative optimization
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