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林4-36X井防漏防窜水泥浆固井技术
引用本文:杨国胜,缪华,苏冀中,秦继涛,周虹,杜爱红,莫仁健,顾庆东.林4-36X井防漏防窜水泥浆固井技术[J].石油钻采工艺,2009,31(Z1).
作者姓名:杨国胜  缪华  苏冀中  秦继涛  周虹  杜爱红  莫仁健  顾庆东
作者单位:1. 华北油田公司,河北任丘,062552
2. 华北油田公司天成实业集团有限公司,河北任丘,062552
3. 渤海钻探第一固井工程技术公司,河北任丘,062552
摘    要:林4-36X井是二连油田低压区块上的一口开发井,目的层段压力系数0.6~0.9,钻井过程中在油层段1372.4 m和1485.3 m处发生漏失,井漏时钻井液密度1.19 g/cm3;在发生井漏的同时,也存在着油水外浸.在井温低、水泥用量小的情况下,采用低密度防漏防窜水泥浆体系固井,通过降低水泥浆密度并在水泥中加入弹性防漏堵漏材料,提高水泥浆的防窜性能等技术措施进行固井,施工作业顺利,电测固井质量优质.

关 键 词:林4-36X井  固井  低密度水泥浆  防漏  防窜

Cementing technology of using leak protection and water shutoff drilling fluid in LIN 4-36X Well
YANG Guosheng,MIU Hua,SU Jizhong,QIN Jitao,ZHOU Hong,DU Aihong,MO Renjian,GU Qingdong.Cementing technology of using leak protection and water shutoff drilling fluid in LIN 4-36X Well[J].Oil Drilling & Production Technology,2009,31(Z1).
Authors:YANG Guosheng  MIU Hua  SU Jizhong  QIN Jitao  ZHOU Hong  DU Aihong  MO Renjian  GU Qingdong
Abstract:LIN 4-36X is a development well located in the low-pressure block of Erlian Oilfield. Pressure coefficient of its target layer is between 0. 3 to 0. 4. In the course of drilling, leakage happened in the positions of 1372. 4m and 1485. 3 m. The fluid density came to 1.19 g/cm3 when leakage and water soak happened. In that condition, low-density drilling fluid for leak protection and water shutoff was used for cementing and the added flexible leak-proof material made the cementing operation become smooth. Electrical logging results showed that the cementing was of high quality.
Keywords:LIN 4-36X Well  cementing  low-density drilling fluid  leak protection  anti-channeling
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