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粘土斜墙堆石坝的渗流反演分析
引用本文:姬志军,段祥宝. 粘土斜墙堆石坝的渗流反演分析[J]. 大坝与安全, 2011, 0(5): 53-58
作者姓名:姬志军  段祥宝
作者单位:河南省豫北水利勘测设计院,河南安阳,455000;南京水利科学研究院,江苏南京,210029
摘    要:小南海水库大坝为粘土斜墙堆石坝,上游为重粉质壤土填筑的厚粘土斜墙,粘土斜墙后紧接堆石坝体,粘土斜墙与堆石体之间设反滤层.坝基以闪长岩为主,原河床位于右坝段,河床段基岩覆盖层厚8~12m,其中强透水性砂卵石层厚3~5 m.坝基防渗工程仅为三道质量不高的截水槽.通过对小南海水库大坝进行渗流分析,找出大坝渗流安全方面存在的问...

关 键 词:粘土斜墙堆石坝  截水槽  渗流分析

Inverse analysis on the seepage of rock-fill dam with inclined clay-core wall
JI Zhi-jun , DUAN Xiang-bao. Inverse analysis on the seepage of rock-fill dam with inclined clay-core wall[J]. Large Dam & Safety, 2011, 0(5): 53-58
Authors:JI Zhi-jun    DUAN Xiang-bao
Affiliation:JI Zhi-jun and DUAN Xiang-bao Hydraulic Engineering Planning and Design Institute of North Henan
Abstract:Xiaonanhai reservoir dam is a rock-fill dam with inclined clay-core wall. The upstream thick inclined clay-core wall was filled with heavy silt loam. The embankment was behind the wall and a filter layer was set between. Diorite filled a large part of dam foundation and the original river bed located on the right. The thickness of dam foundation overburden was 8~12 m, of which the thickness of the strong permeable sand pebble layer was 3~5 m. Seepage prevention works at dam foundation were only 3 cutoff trenches of poor quality. The paper analysed the seepage of Xiaonanhai reservoir dam and pointed out the existing problems, worthy reference for rehabilitation and decision making.
Keywords:rock-fill dam with inclined clay-core wall  cutoff trench  seepage analysis
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