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广州发电厂3号锅炉提高过热汽温的技术措施
引用本文:李建国.广州发电厂3号锅炉提高过热汽温的技术措施[J].华北电力技术,2010(2):33-35.
作者姓名:李建国
作者单位:广州发电厂,广东广州,510160
摘    要:广州发电厂3号锅炉大修后,在额定负荷运行时,过热汽温长期低过530℃,在低负荷运行时,汽温更低,影响锅炉和汽轮机的安全运行,文章分析了3号炉汽温偏低的原因,提出和实施提高过热汽温的技术措施,控制汽温在规程规定的范围内,取到明显的效果。

关 键 词:锅炉  提高汽温  过热汽温  技术措施

Technical Measures for Raising Superheated Steam Temperature of Boiler 3 in Guangzhou Power Plant
Li Jian-guo.Technical Measures for Raising Superheated Steam Temperature of Boiler 3 in Guangzhou Power Plant[J].North China Electric Power,2010(2):33-35.
Authors:Li Jian-guo
Affiliation:Guangzhou Power Plant;Guangzhou 510160;China
Abstract:In Guangzhou Power Plant,the superheated steam temperature of boiler 3 is long-term lower than 530℃ in rated load operation after the overhaul, especially in low - load operation. The situation is concerned to the safety of boiler and steam turbine operation. This paper analyzes the reasons for low steam temperature of boiler 3, then propo- ses and implements some technical measures which can raise superheated steam temperature to control the tempera- ture within the scope of specification, the measures obtain significant results.
Keywords:boiler  raise temperature  superheated steam temperature  technical measure  
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