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复合生物反应器亚硝酸型同步硝化反硝化脱氮
引用本文:王建龙,彭永臻,王淑莹,高永青.复合生物反应器亚硝酸型同步硝化反硝化脱氮[J].中国化学工程学报,2008,16(5):778-784.
作者姓名:王建龙  彭永臻  王淑莹  高永青
作者单位:College of Environmental and Energy Engineering, Beijing University of Technology, Beijing 100022, China
基金项目:National Key Project of Scientifc and Technical Supporting Program of Ministry of Science and Technology of China,Academic Human Resources Development in Institutions of Higher Leading under the Jurisdiction of Beijing Municipality,高等学校博士学科点专项科研项目
摘    要:Sequence hybrid biological reactor (SHBR) was proposed, and some key control parameters were investigated for nitrogen removal from wastewater by simultaneous nitrification and denitrification (SND) via nitrite. SND via nitrite was achieved in SHBR by controlling demand oxygen (DO) concentration. There was a programmed decrease of the DO from 2.50 mg·L^-1 to 0.30 mg·L^-1, and the average nitrite accumulation rate (NAR) was increased from 16.5% to 95.5% in 3 weeks. Subsequently, further increase in DO concentration to 1.50 mg·L^-1 did not destroy the partial nitrification to nitrite. The results showed that limited air flow rate to cause oxygen deficiency in the reactor would eventually induce only nitrification to nitrite and not further to nitrate. Nitrogen removal efficiency was increased with the increase in NAR, that is, NAR was increased from 60% to 90%, and total nitrogen removal efficiency was increased from 68% to 85%. The SHBR could tolerate high organic loading rate (OLR), COD and ammonia-nitrogen removal efficiency were greater than 92% and 93.5%, respectively,, and it even operated under low DO concentration (0.5 mg·L^-1) and maintained high OLR (4.0 kg COD·m^-3·d^-1). The presence of biofilm positively affected the activated sludge settling capability, and sludge volume index (SVI) of activated sludge in SHBR never hit more than 90 ml·L^-1 throughout the experiments.

关 键 词:nitrogen  removal  simultaneous  nitrification  and  denitrification  nitrite  accumulation  demand  oxygen  pH  
收稿时间:2007-10-18
修稿时间:2008-4-20  

Nitrogen removal by simultaneous nitrification and denitrification via nitrite in a sequence hybrid biological reactor
WANG Jianlong,PENG Yongzhen,WANG Shuying,GAO Yongqing.Nitrogen removal by simultaneous nitrification and denitrification via nitrite in a sequence hybrid biological reactor[J].Chinese Journal of Chemical Engineering,2008,16(5):778-784.
Authors:WANG Jianlong  PENG Yongzhen  WANG Shuying  GAO Yongqing
Affiliation:College of Environmental and Energy Engineering, Beijing University of Technology, Beijing 100022, China
Abstract:Sequence hybrid biological reactor(SHBR)was proposed,and some key control parameters were in-vestigated for nitrogen removal from wastewater by simultaneous nitrification and denitrification(SND)via nitrite.sND via nitrite was achieved in SHBR by controlling demand oxygen(DO)concentration.There was a pro-did not destroy the partial nitrification to nitrite.The results showed that limited air flow rate to cause oxygen defi-ciency in the reactor would eventually induce only nitrification to nitrite and not further to nitrate.Nitrogen removal efficiency was increased with the increase in NAR,that iS,NAR was increased from 60%to 90%,and total nitrogen removal efficiency was increased from 68%t0 85%.The SHBR could tolerate high organic loading rate(OLR),COD and ammonia-nitrogen removal efficiency were greater than92%and 93.5%respectively and it even oper-biofilm positively affected the activated sludge settling capability,and sludge volume index(svi)of activated sludge in SHBR never hit more than 90 ml.g-1 throughout the experiments.
Keywords:nitrogen removal  simultaneous nitrification and denitrihCaoon  nitrite accumulation  demand oxygen  pH
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