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水力振荡器在大位移井张海29-38L井的应用
引用本文:许京国,陶瑞东,杨静,张连水,张建荣,王永路,杨杰.水力振荡器在大位移井张海29-38L井的应用[J].断块油气田,2014(4):527-529.
作者姓名:许京国  陶瑞东  杨静  张连水  张建荣  王永路  杨杰
作者单位:中国石油渤海钻探工程公司第三钻井工程公司,天津300280
基金项目:中国石油渤海钻探公司科技攻关项目“成熟钻井技术集成配套研究与应用”(2013ZD18Y)
摘    要:张海29-38L井是部署在埕海2-2人工岛的一口三开大位移定向井,最大水平位移2 625.38 m,最大井斜76.24.,三开滑动钻进井段频繁出现托压、压差卡钻现象.于是尝试应用了水力振荡器,其工作原理是通过自身产生的纵向振动,来提高滑动钻进过程中钻压传递的有效性和减少钻具与井壁之间的摩阻.张海29-38L井应用结果表明,应用水力振荡器井段比未使用该工具井段的机械钻速提高了218%,提速效果非常显著.水力振荡器在该井的成功应用,为探索大位移井钻井提速提供了有益的借鉴.

关 键 词:水力振荡器  钻压  机械钻速  大位移井  托压  摩阻  大港油田

Application of hydraulic oscillator in Zhanghai 29-38L extended reach well
Xu JingguoNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Tao RuidongNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Yang JingNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Zhang LianshuiNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Zhang JianrongNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Wang YongluNo.,Drilling Company,Bohai Drilling Engineering Company Limited,CNPC,Tianjin,China Yang Jie.Application of hydraulic oscillator in Zhanghai 29-38L extended reach well[J].Fault-Block Oil & Gas Field,2014(4):527-529.
Authors:Xu JingguoNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Tao RuidongNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Yang JingNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Zhang LianshuiNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Zhang JianrongNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Wang YongluNo  Drilling Company  Bohai Drilling Engineering Company Limited  CNPC  Tianjin  China Yang Jie
Affiliation:Xu Jingguo(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Tao Ruidong(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Yang Jing(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Zhang Lianshui(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Zhang Jianrong(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Wang Yonglu(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China) Yang Jie(No.3 Drilling Company, Bohai Drilling Engineering Company Limited, CNPC, Tianjin 300280, China)
Abstract:Well Zhanghai 29-38L is deployed in Chenghai 2-2 artificial island as extended reach well with horizontal displacement of 2,625.38 m,maximum inclination of 76.24°.Backing pressure and differential pressure sticking frequently occur during the third-spud sliding drilling,so the hydraulic oscillator is tried to be used,whose working principle is the longitudinal vibration by itself to improve the effective transmission of sliding drilling WOB and reduce the friction between the drill string and borehole wall.The results of field application show that compared with the well section no use of this tool,in the well section used hydraulic oscillator,ROP is increased by 218%,getting very significant effect; the successful application of hydraulic oscillator in Well Zhanghai 29-38L provides the beneficial reference for the penetration rate raising of extended reach well.
Keywords:hydraulic oscillator  WOB  ROP  extended reach well  backing pressure  friction  Dagang Oilfield
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