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10Cr21Mnl6NiN不锈钢冶炼与连铸生产实践
引用本文:张增武. 10Cr21Mnl6NiN不锈钢冶炼与连铸生产实践[J]. 特殊钢, 2020, 41(3): 47-50
作者姓名:张增武
作者单位:山西太钢不锈钢股份有限公司炼钢二厂,太原030003
摘    要:通过对10Cr21Mn16NiN高氮不锈钢冶炼和连铸工艺研究,在生产中改进两步法冶炼和连铸生产工艺,与三步法工艺相比,LF精炼后期增氮速度由5×10-6~10×10-6/min提高到20×10-6~30×10-6/min,LF精炼时间由390 min缩短至240 min,连铸等钢时间由4 h降至2 h以下;解决了钢包增氮炉渣外溢的问题;避免了方坯在连铸过程中的翘头,No.1、No.2流断浇率由开发时100%降至0,设备事故率由66.7%降至0,2炉连浇率实现100%。实践证明,方坯连铸机辊子非密排且仅有1台五辊拉矫机也能生产出高强不锈钢方坯。

关 键 词:高猛高氮不锈钢10Cr21Mnl6NiN  增氮  溢渣  翘头  方坯连铸  
收稿时间:2019-12-28

Smelting and Continuous Casting Practice of Stainless Steel 10Cr21Mnl6NiN
Zhang Zengwu. Smelting and Continuous Casting Practice of Stainless Steel 10Cr21Mnl6NiN[J]. Special Steel, 2020, 41(3): 47-50
Authors:Zhang Zengwu
Affiliation:No. 2 Steelmaking Plant of Shanxi Taigang Stainless Steel Co. Ltd, Taiyuan 030003
Abstract:Compare with the three-step method, through the study of smelting and continuous casting of High-Nitrogen stainless steel 10Cr21 Mnl6NiN, the two-step smelting and continuous casting technology has been optimized, the adding nitrogen rate is raised from 5 x 10 -6 ~ 10 x 10-6/min to 20 x 10-6~ 30 x 10 -6/min in later stages of LF, the LF refining time is shortened from 390 min to 240 min, the CCM steel waiting time is reduced from 4 h to 2 h ; it solves the problem of slag spilling during the nitrogen adding;it also avoids the billet buckling during continuous casting,the breakage rate of No. 1 & No. 2 casting strand reduces from 100% to O,the equipment accident rate decreases from 66. 7% to 0,to achieve 100% 2- heats sequence casting. The practice shows that the billet casting without closely spaced rolls can produced High-Nitrogen stainless steel even though with only one five-high withdrawing and straightening machine.
Keywords:High-Nitrogen  High-Manganese Stainless Steel 10Cr21 Mnl6NiN   Adding Nitrogen   Slag Spilling   Buckling   Continuous Casting Billet  
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