汽柴油加氢装置催化剂性能考察及长周期运行操作优化 |
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引用本文: | 李丽蓉 袁小彬. 汽柴油加氢装置催化剂性能考察及长周期运行操作优化[J]. 石油炼制与化工, 2020, 51(11): 35-39 |
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作者姓名: | 李丽蓉 袁小彬 |
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作者单位: | 中国石化塔河炼化有限责任公司 |
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摘 要: | 为了适应柴油产品质量升级需求,中国石化塔河炼化公司2号汽柴油加氢装置采用中国石化石油化工科学研究院开发的RS2100/RS2110超深度加氢脱硫催化剂新鲜剂和中国石化大连(抚顺)石油化工研究院开发的FHUDS系列催化剂再生剂,处理焦化汽油、焦化柴油和常二线柴油的混合原料,得到的精制柴油硫质量分数为3.2 μg/g,氮质量分数为0.67 μg/g,多环芳烃质量分数为2.9%,十六烷值为52,闪点(闭口)为68 ℃,满足国Ⅵ柴油质量升级的要求。装置运行不到一年,催化剂失活速率大于24.0 ℃/a,而后通过调整两台反应器的温度分布、原料组成和产品硫含量,使催化剂失活速率小于14.4 ℃/a,反应器床层最高温度不大于390 ℃,反应器压差维持在0.4 MPa,催化剂稳定性较好,能够满足装置长周期运行的要求。
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关 键 词: | 加氢催化剂 焦化汽油 焦化柴油 加氢脱硫 操作优化 国Ⅵ柴油 |
收稿时间: | 2020-04-21 |
修稿时间: | 2020-06-12 |
OPTIMIZATION AND LONG TERM OPERATION OF GASOLINE AND DIESEL HYDROTREATING UNIT |
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Abstract: | The fresh ultra-deep hydrodesulfurization catalysts RS2100/RS2110 (developped by SINOPEC Research Institute of Petroleum Processing) and regenerated FHUDS catalyst series (developped by SINOPEC Dalian(Fushun) Research Institute of Petroleum Processing) were used in a 1.67 Mt/a hydrotreating unit processing mixed feedstock of coker gasoline, coker diesel and atmospheric gas oil in SINOPEC Tahe Refinery & Chemical Company. The national VI standard diesel was obtained with flash point (closed) of 68℃,S content of 3.2 μg/g,nitrogen content of 0.67 μg/g, cetane number of 52,and poly-aromatic hydrocarbons content of 2.9 %. However, the deactivation rate of catalysts was to 24.0 ℃/a within half a year. After adjusting the temperature distribution of two reactors,raw material composition as well as the sulfur content of products, the catalyst deactivation rate was reduced to less than 14.4 ℃/a,the pressure drop of reactors was 0.4 MPa, and the maximum temperature of reactor bed was less than 390 ℃, indicating a good stability of the catalysts system. The catalysts can meet the need for long term operation. |
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Keywords: | hydrogenation catalysts coker gasoline coker diesel hydrodesulfurization operation optimization China national standard Ⅵ diesel |
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